Forced Induction Superchargers | Turbochargers | Intercoolers

Im about to pull my damn hair out

Thread Tools
 
Search this Thread
 
Old 07-20-2007, 10:18 PM
  #1  
TECH Enthusiast
Thread Starter
iTrader: (25)
 
1fstTA's Avatar
 
Join Date: Nov 2001
Location: shreveport, Louisiana
Posts: 648
Likes: 0
Received 0 Likes on 0 Posts

Default Im about to pull my damn hair out

Man we have been fighting a stumbling problem right when the car is coming on hard at about 5500 and I dont know what the hell is going on. The car is popping and stumbling once you get it in the upper rpms any ideas. Programming with bs3 I can post up logs to anyone that has a idea
Old 07-21-2007, 07:34 AM
  #2  
TECH Senior Member
iTrader: (59)
 
MIGHTYMOUSE's Avatar
 
Join Date: Nov 2001
Location: Virginia
Posts: 10,010
Received 45 Likes on 31 Posts

Default

not enough timing, wrong plug, wrong plug gap, weak coil(s), plug wires, too much octane, too much fuel

interesting this popped up because out of nowhere my car did this last night.

i was hoping in my case it was a fouled wideband.. but that doesnt seem to be the case....i have filled it back up with 93 (had 5 gal of 1100) and it seems to be clearing up.. weird.
Old 07-21-2007, 08:27 AM
  #3  
FormerVendor
 
qqwqeqwrqwqtq's Avatar
 
Join Date: Dec 2001
Location: WWW.SPEEDINC.COM
Posts: 2,444
Likes: 0
Received 2 Likes on 2 Posts

Default

Try disabling the cam sync error test for a run.
Old 07-21-2007, 08:52 AM
  #4  
On The Tree
iTrader: (-1)
 
jegan1989's Avatar
 
Join Date: Jul 2006
Location: DETROIT MI
Posts: 114
Likes: 0
Received 0 Likes on 0 Posts

Default

[QUOTE=MIGHTYMOUSE]not enough timing, wrong plug, wrong plug gap, weak coil(s), plug wires, too much octane, too much fuel

what is the hosepower you are putting out because it could be any of these problems and all of the those parts that mightymouse had named they all peak out at a highhorse power range or over peak with the fuel
Old 07-21-2007, 11:18 AM
  #5  
TECH Enthusiast
Thread Starter
iTrader: (25)
 
1fstTA's Avatar
 
Join Date: Nov 2001
Location: shreveport, Louisiana
Posts: 648
Likes: 0
Received 0 Likes on 0 Posts

Default

Im going back to mess with it today and play with it. I just got the car running and Ive got a baseline tune we havent had it on the rollers yet. Im running c16. Its got us stumped. Ill try disabling the cam sync and see what is going on. My plan is to take it to Mike Morillo and have him do his magic on the car but I wanted to make sure the care is sound before I make that haul.
Old 08-10-2007, 09:06 PM
  #6  
TECH Regular
iTrader: (2)
 
KissMySSo1's Avatar
 
Join Date: Jul 2004
Posts: 494
Likes: 0
Received 1 Like on 1 Post

Default

ever have any luck with this?
Old 08-11-2007, 10:23 AM
  #7  
TECH Enthusiast
Thread Starter
iTrader: (25)
 
1fstTA's Avatar
 
Join Date: Nov 2001
Location: shreveport, Louisiana
Posts: 648
Likes: 0
Received 0 Likes on 0 Posts

Default

Yea I had the plugs gaped to big and I also had a problem with one of the msd coils. Now Im having gasket problems. The car is pushing water very bad but it did make it on the dyno to 28lbs
Old 08-11-2007, 12:01 PM
  #8  
TECH Junkie
iTrader: (9)
 
bboyferal's Avatar
 
Join Date: Apr 2005
Location: Miami, FL
Posts: 3,472
Likes: 0
Received 0 Likes on 0 Posts

Default

DAMN, well I'll say it didn't do too bad then!
Old 08-11-2007, 03:53 PM
  #9  
9 Second Club
iTrader: (35)
 
ninetres's Avatar
 
Join Date: Nov 2005
Location: Mufflerville, CA
Posts: 3,128
Likes: 0
Received 4 Likes on 4 Posts
Default

Originally Posted by 1fstTA
Yea I had the plugs gaped to big and I also had a problem with one of the msd coils. Now Im having gasket problems. The car is pushing water very bad but it did make it on the dyno to 28lbs
What plugs and what was the before and after gap?

My car did this as well for about a week before it seized up. I tried both TR6s gapped at .035 then .030, and then I switched to a TR7 and it sputtered both at .030 and .025 still.

104 octane BTW.
Old 08-11-2007, 04:04 PM
  #10  
TECH Enthusiast
Thread Starter
iTrader: (25)
 
1fstTA's Avatar
 
Join Date: Nov 2001
Location: shreveport, Louisiana
Posts: 648
Likes: 0
Received 0 Likes on 0 Posts

Default

I had TR 6's and they were gapped at .036 I pulled them out and my mechanic and I put 10's and they are gapped at .28. We actually also had 2 msd coils that werent acting right.



Quick Reply: Im about to pull my damn hair out



All times are GMT -5. The time now is 08:30 PM.