Nitrous cutting OUT!!!
#1
TECH Fanatic
Thread Starter
iTrader: (4)
Join Date: Nov 2005
Posts: 1,078
Likes: 0
Received 0 Likes
on
0 Posts
Nitrous Problems!
Hey guys my nitrous has been fine for the past week but all of a sudden when im going it just shorts out and then kicks back on and off repeatedly- i went through and recrimped all connections and covered all in electrical tape- but there is a small leak in the nitrous line between the purge and solenoid- could this cause something? ANY ideas?
Last edited by 02Vortech; 01-18-2006 at 10:50 PM.
#2
Originally Posted by 02Vortech
Hey guys my nitrous has been fine for the past week but all of a sudden when im going it just shorts out and then kicks back on and off repeatedly- i went through and recrimped all connections and covered all in electrical tape- but there is a small leak in the nitrous line between the purge and solenoid- could this cause something? ANY ideas?
#5
Closed ex-Sponsor Account
iTrader: (1)
Join Date: Jul 2004
Location: Wichita Falls, TX
Posts: 2,797
Likes: 0
Received 0 Likes
on
0 Posts
ON and off while driving or just testing with your pushing the wot switch. The reason I ask, if your seat is too far back when you launch it could lift off the pedal and you would not know it.
If while testing the relay sounds like it has a bad ground.
Ricky
If while testing the relay sounds like it has a bad ground.
Ricky
Trending Topics
#8
Teching In
iTrader: (2)
Join Date: Sep 2004
Location: Rome Georgia
Posts: 3
Likes: 0
Received 0 Likes
on
0 Posts
Mine pulsed like that one time. My wot switch was too sensitive and was clicking on and off. I adjusted it to come on sooner or easier and it fixed the problem. Might help to check it.
#9
TECH Fanatic
Thread Starter
iTrader: (4)
Join Date: Nov 2005
Posts: 1,078
Likes: 0
Received 0 Likes
on
0 Posts
mine comes on pretty easily (WOT switch)- im gonna put my money on that it is the leak in the purge fitting causing my problem along w/ low bottle pressure- the leak is noticable w/ hood down and engine running so im prolly loosing 100 to 200psi when its leaking which is bad to say the least.... so im gonna fix that saturday along w/ put on the bottle heater i hope!
well i got low bottle pressure and a small leak and alot of people are saying that low psi causes surging- and i will move the seat up farther- also the zex bottle mounts i think are a little low im gonna put a mount on the bottom of the front one to set it up a little higher- also im gonna replace the leaky fitting and get the bottle warmer and blanket on there and run 1000psi and see what happens then-
well i got low bottle pressure and a small leak and alot of people are saying that low psi causes surging- and i will move the seat up farther- also the zex bottle mounts i think are a little low im gonna put a mount on the bottom of the front one to set it up a little higher- also im gonna replace the leaky fitting and get the bottle warmer and blanket on there and run 1000psi and see what happens then-
Last edited by 02Vortech; 01-19-2006 at 02:51 PM.
#10
10 Second Club
iTrader: (2)
Join Date: Dec 2004
Location: Sumter, South Carolina
Posts: 1,386
Likes: 0
Received 1 Like
on
1 Post
Originally Posted by 02Vortech
mine comes on pretty easily (WOT switch)- im gonna put my money on that it is the leak in the purge fitting causing my problem along w/ low bottle pressure- the leak is noticable w/ hood down and engine running so im prolly loosing 100 to 200psi when its leaking which is bad to say the least.... so im gonna fix that saturday along w/ put on the bottle heater i hope!
well i got low bottle pressure and a small leak and alot of people are saying that low psi causes surging- and i will move the seat up farther- also the zex bottle mounts i think are a little low im gonna put a mount on the bottom of the front one to set it up a little higher- also im gonna replace the leaky fitting and get the bottle warmer and blanket on there and run 1000psi and see what happens then-
well i got low bottle pressure and a small leak and alot of people are saying that low psi causes surging- and i will move the seat up farther- also the zex bottle mounts i think are a little low im gonna put a mount on the bottom of the front one to set it up a little higher- also im gonna replace the leaky fitting and get the bottle warmer and blanket on there and run 1000psi and see what happens then-
If it's not a leak...It still "sounds" electrical by your description. There really arn't that many places that you need to check. I really suggest that anyone who messes with electrical use a multi meter to check voltages. Maybe draw out a schematic of exactly what you have scan and upload it somewhere to be seen...it will benefit you and us to help you troubleshoot your system.
#11
TECH Fanatic
Thread Starter
iTrader: (4)
Join Date: Nov 2005
Posts: 1,078
Likes: 0
Received 0 Likes
on
0 Posts
okay if isnt the pressure and leak i will do that for you- here is how it should be- its to dark out to go look so this is how i remember it-
sorry i resized it but photobucket isnt regestering it-
sorry i resized it but photobucket isnt regestering it-
Last edited by 02Vortech; 01-19-2006 at 09:48 PM.
#12
10 Second Club
iTrader: (2)
Join Date: Dec 2004
Location: Sumter, South Carolina
Posts: 1,386
Likes: 0
Received 1 Like
on
1 Post
Originally Posted by 02Vortech
okay if isnt the pressure and leak i will do that for you- here is how it should be- its to dark out to go look so this is how i remember it-
sorry i resized it but photobucket isnt regestering it-
sorry i resized it but photobucket isnt regestering it-
#13
TECH Fanatic
Thread Starter
iTrader: (4)
Join Date: Nov 2005
Posts: 1,078
Likes: 0
Received 0 Likes
on
0 Posts
OKAY WTF-
heres the deal-
i ran the truck this morning on a 75 shot and it worked good the first two times then it started cutting out again- so i go home check all the grounds and recrimp everything and put them back- then tonight i try to spray and it wont spray at all- i had the switch turned on half a bottle of nitrous and 890psi- so do yall think its the msd window switch f'n up on me?
heres the deal-
i ran the truck this morning on a 75 shot and it worked good the first two times then it started cutting out again- so i go home check all the grounds and recrimp everything and put them back- then tonight i try to spray and it wont spray at all- i had the switch turned on half a bottle of nitrous and 890psi- so do yall think its the msd window switch f'n up on me?
#14
TECH Senior Member
iTrader: (2)
Originally Posted by 02Vortech
OKAY WTF-
heres the deal-
i ran the truck this morning on a 75 shot and it worked good the first two times then it started cutting out again- so i go home check all the grounds and recrimp everything and put them back- then tonight i try to spray and it wont spray at all- i had the switch turned on half a bottle of nitrous and 890psi- so do yall think its the msd window switch f'n up on me?
heres the deal-
i ran the truck this morning on a 75 shot and it worked good the first two times then it started cutting out again- so i go home check all the grounds and recrimp everything and put them back- then tonight i try to spray and it wont spray at all- i had the switch turned on half a bottle of nitrous and 890psi- so do yall think its the msd window switch f'n up on me?
Robert
#15
TECH Fanatic
Thread Starter
iTrader: (4)
Join Date: Nov 2005
Posts: 1,078
Likes: 0
Received 0 Likes
on
0 Posts
Originally Posted by Robert56
Is it the digital one, if so, it seems to be somewhat problematic. I run a couple of the pill type and they have been flawless.
Robert
Robert
like this?
http://www.msdignition.com/rpm_7.htm
Last edited by 02Vortech; 01-21-2006 at 11:59 PM.