Simple LS Swap Gone Awry (370/LS3 heads/PT88)
#162
9 Second Club
iTrader: (19)
^ Ain't that the truth. You can't even hear my cam now that I have full exhaust. It is seriously as quiet as a stock Fbody. Had a guy in a C5 try to run me from a stop light the other night. I eased into it and let him get out a head a bit, then matted it and flew past him like he was standing still. He came up to me at the next light and asked what the hell just happened.
Your car is a little nastier than mine though.
Your car is a little nastier than mine though.
#173
Had it at the track yesterday. My launch needs a lot of work... the car won't hold itself. It just pushes the front tires because the stock rear brakes won't hold it. The highest RPM I could leave at was 2500 which gave me my best 60' of a 2.16. That same run the car went 11.749 @ 138 mph. The boost was set at 17 for that pass and I eased into it a lot more gradual than most passes. The biggest issue was that about 300 feet out the car lost traction half of the time. Pulled off an 11.80 @ 131 on 10psi once (forgot to turn up the boost controller on that pass).
My goal was to go 10.99 or 130 mph (or both) so I was happy with the mph! If I could get the 60' down and floor it a little sooner It should run the ET eventually. It was still a fun day to kind of figure out what the car would do.
Only had a couple problems and the rear end wasn't one of them! One of the nuts backed off on the manifolds... wish I had just done vbands! The other problem was on the final pass the car just wouldn't make boost. It was time to go home anyway so we just loaded it up on the trailer and while looking underneath it noticed that the IC pipe had come out of the coupler on the hot side of the intercooler... This car is a turd out of boost!!!
Working on getting the videos uploaded now. Maybe I'll get them posted some time this week. Also want to check out the tune and see where the timing is at down low since it feels like it takes so long to spool.
My goal was to go 10.99 or 130 mph (or both) so I was happy with the mph! If I could get the 60' down and floor it a little sooner It should run the ET eventually. It was still a fun day to kind of figure out what the car would do.
Only had a couple problems and the rear end wasn't one of them! One of the nuts backed off on the manifolds... wish I had just done vbands! The other problem was on the final pass the car just wouldn't make boost. It was time to go home anyway so we just loaded it up on the trailer and while looking underneath it noticed that the IC pipe had come out of the coupler on the hot side of the intercooler... This car is a turd out of boost!!!
Working on getting the videos uploaded now. Maybe I'll get them posted some time this week. Also want to check out the tune and see where the timing is at down low since it feels like it takes so long to spool.
#174
9 Second Club
iTrader: (19)
I am kicking myself for not making the trip up now. Sounds like it was a good time. I am going up the 29th for sure to get some test passes in.
I assume you aren't able to build any boost on the footbrake then? I can build 6 lbs. or so on the street before the tires start to break loose. Did you try just flashing the converter at all and not bringing it up?
I assume you aren't able to build any boost on the footbrake then? I can build 6 lbs. or so on the street before the tires start to break loose. Did you try just flashing the converter at all and not bringing it up?
#175
9 Second Club
iTrader: (33)
Had it at the track yesterday. My launch needs a lot of work... the car won't hold itself. It just pushes the front tires because the stock rear brakes won't hold it. The highest RPM I could leave at was 2500 which gave me my best 60' of a 2.16. That same run the car went 11.749 @ 138 mph. The boost was set at 17 for that pass and I eased into it a lot more gradual than most passes. The biggest issue was that about 300 feet out the car lost traction half of the time. Pulled off an 11.80 @ 131 on 10psi once (forgot to turn up the boost controller on that pass).
My goal was to go 10.99 or 130 mph (or both) so I was happy with the mph! If I could get the 60' down and floor it a little sooner It should run the ET eventually. It was still a fun day to kind of figure out what the car would do.
Only had a couple problems and the rear end wasn't one of them! One of the nuts backed off on the manifolds... wish I had just done vbands! The other problem was on the final pass the car just wouldn't make boost. It was time to go home anyway so we just loaded it up on the trailer and while looking underneath it noticed that the IC pipe had come out of the coupler on the hot side of the intercooler... This car is a turd out of boost!!!
Working on getting the videos uploaded now. Maybe I'll get them posted some time this week. Also want to check out the tune and see where the timing is at down low since it feels like it takes so long to spool.
My goal was to go 10.99 or 130 mph (or both) so I was happy with the mph! If I could get the 60' down and floor it a little sooner It should run the ET eventually. It was still a fun day to kind of figure out what the car would do.
Only had a couple problems and the rear end wasn't one of them! One of the nuts backed off on the manifolds... wish I had just done vbands! The other problem was on the final pass the car just wouldn't make boost. It was time to go home anyway so we just loaded it up on the trailer and while looking underneath it noticed that the IC pipe had come out of the coupler on the hot side of the intercooler... This car is a turd out of boost!!!
Working on getting the videos uploaded now. Maybe I'll get them posted some time this week. Also want to check out the tune and see where the timing is at down low since it feels like it takes so long to spool.
#176
Tonight I went for a ride with a friend and he suggested the possibility of the intercooler pipe that was popped off might have been leaking boost all day. After him saying that I was doing some street launching and it seemed to be much more responsive than I remember at the track... How likely is it that the junction was leaking boost before it came undone all the way? Now I'm getting anxious to go back!
Footbrake won't build any boost. Did not try flashing the converter.
CFR
I am kicking myself for not making the trip up now. Sounds like it was a good time. I am going up the 29th for sure to get some test passes in.
I assume you aren't able to build any boost on the footbrake then? I can build 6 lbs. or so on the street before the tires start to break loose. Did you try just flashing the converter at all and not bringing it up?
I assume you aren't able to build any boost on the footbrake then? I can build 6 lbs. or so on the street before the tires start to break loose. Did you try just flashing the converter at all and not bringing it up?
CFR
#177
9 Second Club
iTrader: (19)
I'd say it's possible that it could have been leaking before it came undone. Did you have a chance to log your runs? That should show what your KPA/Boost was doing under load obviously. The only coupler I have blown off was the one that attaches to the TB. It never had a chance to leak as I knew as soon as it popped off.
Strange about not being able to build anything on the footbrake. We both have Circle D converters and sounds like they behave completely different. I realize we both have different setups, gears, etc., but would think you should be able to build some boost on the footbrake. Might want to give the flash a try. Not sure if you seen the video of the guy in the stock looking Z28 with a PT88, but he just flashed the converter and was cutting 1.7 60's on 255/50/16 Mickeys on his way to a 9.98 @ 140. Your car definitely has a 9 second pass in it and a 1.7 60' on a 10 bolt shouldn't be a problem...I hope, haha.
Head back down the 29th! I will be there for sure that day.
Strange about not being able to build anything on the footbrake. We both have Circle D converters and sounds like they behave completely different. I realize we both have different setups, gears, etc., but would think you should be able to build some boost on the footbrake. Might want to give the flash a try. Not sure if you seen the video of the guy in the stock looking Z28 with a PT88, but he just flashed the converter and was cutting 1.7 60's on 255/50/16 Mickeys on his way to a 9.98 @ 140. Your car definitely has a 9 second pass in it and a 1.7 60' on a 10 bolt shouldn't be a problem...I hope, haha.
Head back down the 29th! I will be there for sure that day.
#178
I never heard the coupler come off. It just happened to be off on my next pass. I wish I knew for sure. No logs of the runs. Next time I go I plan to log though. I still haven't tried to build boost but last night I was able to stall it another 500-600 rpm on the street without pushing the front tires. It felt FAST last night especially as soon as it shifted into second. Saturday it was just lazy when it shifted into second.
I need to redo the manifold collector gaskets... Got a nice tick because the passenger side blew one out. Suppose that could contribute to a boost leak as well. If I continue to have problems with that area of the turbo kit (bolts/gaskets) I will probably redo the hot side this winter with v bands and smaller pipe.
I need to redo the manifold collector gaskets... Got a nice tick because the passenger side blew one out. Suppose that could contribute to a boost leak as well. If I continue to have problems with that area of the turbo kit (bolts/gaskets) I will probably redo the hot side this winter with v bands and smaller pipe.
#179
9 Second Club
iTrader: (19)
The first time I built boost on the footbrake my u-joint snapped in half, ha. It was a cheap replacement that I got in a pinch and it scared the crap out of me when it happened.
I am anxious to see what mine feels like when I can actually go WOT in 1st. Right now if I ease into it from a dig I can get it to pull to 5k or so with little tire spin before it shifts. 2nd gear is just crazy though. I can only imagine what your car must feel like with a bigger, better turbo!
FWIW I just used high temp RTV as gaskets and don't have any leaks.
I will probably redo my hotside this winter to make room for a bigger turbo if my LQ4 is still running. I told myself I would be happy with ~650 rwhp, but I already want more. I want to get my trans freshened up, as well as get a 9 inch under the car too.
I am anxious to see what mine feels like when I can actually go WOT in 1st. Right now if I ease into it from a dig I can get it to pull to 5k or so with little tire spin before it shifts. 2nd gear is just crazy though. I can only imagine what your car must feel like with a bigger, better turbo!
FWIW I just used high temp RTV as gaskets and don't have any leaks.
I will probably redo my hotside this winter to make room for a bigger turbo if my LQ4 is still running. I told myself I would be happy with ~650 rwhp, but I already want more. I want to get my trans freshened up, as well as get a 9 inch under the car too.
#180
I used RTV last time and it leaked so I bought the copper gaskets that SCE sells and even put a bead of RTV around them and it blew them out. Not sure how though.... almost looks like they melted.
Here is the video of that 10 lb pass that seemed to go the best of all the passes I made.
Here is the video of that 10 lb pass that seemed to go the best of all the passes I made.