Lost close to 100rwhp through drivetrain: What could've caused it?
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Lost close to 100rwhp through drivetrain: What could've caused it?
Can a rediculously overfilled tranny cause such a breakdown in hydraulics to cause that much
drag? Or was my Torque Converter bad?
My engine threw a rod on the highway so I replaced it with a new shortblock. I put back in my
Vig3200, and went for a drive. I had a strange hollow-rubbing noise coming from the tranny
area that could only be heard from inside the car.
I went to the dyno and only pulled 283rwhp, down from 321rwhp, pre- cam!!
Now, I messed up and overfilled the tranny. I mean absolutely overfilled it. I assumed I had lost
just that much fluid. When the Vig was being pulled fluid was shooting out the tail when the
driveshaft was taken out. <img border="0" title="" alt="[Embarrassed]" src="gr_emb.gif" /> As well as anytime the tranny was moved.
So could it be the fluid causing the loss, or a bad TC. Now that my stocker is back in, I'm
back in the high 3XX rwhp.
Any theories?
drag? Or was my Torque Converter bad?
My engine threw a rod on the highway so I replaced it with a new shortblock. I put back in my
Vig3200, and went for a drive. I had a strange hollow-rubbing noise coming from the tranny
area that could only be heard from inside the car.
I went to the dyno and only pulled 283rwhp, down from 321rwhp, pre- cam!!
Now, I messed up and overfilled the tranny. I mean absolutely overfilled it. I assumed I had lost
just that much fluid. When the Vig was being pulled fluid was shooting out the tail when the
driveshaft was taken out. <img border="0" title="" alt="[Embarrassed]" src="gr_emb.gif" /> As well as anytime the tranny was moved.
So could it be the fluid causing the loss, or a bad TC. Now that my stocker is back in, I'm
back in the high 3XX rwhp.
Any theories?
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Re: Lost close to 100rwhp through drivetrain: What could've caused it?
</font><blockquote><font size="1" face="Verdana, Helvetica, sans-serif">quote:</font><hr /><font size="2" face="Verdana, Helvetica, sans-serif">Originally posted by MIGHTYMOUSE:
<strong>i would have the trans checked out, may have messed something up inside it when the motor went</strong></font><hr /></blockquote><font size="2" face="Verdana, Helvetica, sans-serif">If that was the case why am I making mucho power with the stocker back in? I think either I had WAAAAAYAYYYYY too much fluid or the torque converter is bad. I'm just trying to get some opinions on wheter it could've been the fluid.
I really don't want to spend anymore money on another TC
<strong>i would have the trans checked out, may have messed something up inside it when the motor went</strong></font><hr /></blockquote><font size="2" face="Verdana, Helvetica, sans-serif">If that was the case why am I making mucho power with the stocker back in? I think either I had WAAAAAYAYYYYY too much fluid or the torque converter is bad. I'm just trying to get some opinions on wheter it could've been the fluid.
I really don't want to spend anymore money on another TC
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Re: Lost close to 100rwhp through drivetrain: What could've caused it?
what does the torque curve look like on the dyno? does it just go up a little then flat line across? if so I would say your slipping.
Ozz
Ozz
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Re: Lost close to 100rwhp through drivetrain: What could've caused it?
</font><blockquote><font size="1" face="Verdana, Helvetica, sans-serif">quote:</font><hr /><font size="2" face="Verdana, Helvetica, sans-serif">Originally posted by JC:
<strong>I had a strange hollow-rubbing noise coming from the tranny area that could only be heard from inside the car.
</strong></font><hr /></blockquote><font size="2" face="Verdana, Helvetica, sans-serif">I had that same noise that could only be heard in the car, mostly with the windows up. It turned out to be the BMR Loop rubbuing slightly on the torque arm.
<strong>I had a strange hollow-rubbing noise coming from the tranny area that could only be heard from inside the car.
</strong></font><hr /></blockquote><font size="2" face="Verdana, Helvetica, sans-serif">I had that same noise that could only be heard in the car, mostly with the windows up. It turned out to be the BMR Loop rubbuing slightly on the torque arm.
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Re: Lost close to 100rwhp through drivetrain: What could've caused it?
From what I understand the 4L60-E cannot be overfilled as long as the vent tube isn't kinked/clogged. The fluid will just heat up/expand and overfill will expand out the vent tube.
On my car the vent tube is clipped to the torque arm.
Happy driving,
Bad30th
On my car the vent tube is clipped to the torque arm.
Happy driving,
Bad30th