The flat spot.
Last edited by MjMaro; Jan 20, 2010 at 12:01 PM.
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I eventually had the car dyno'd. It was immediately apparent that the car was low on power, and running very lean. Unplugging the MAF net a 25 HP increase and it was now running quite rich. We removed and cleaned the MAF, and the car ran even stronger, likely due to not being so rich. Didn't get a chance to dyno it again though. The 'flat spot' was forever gone.
The PO had used a K&N Filter, and had over-oiled it. The excess oil got pulled off into the intake stream and coated the MAF, leading to incorrect readings and hence incorrect A/F ratio.
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The PO had used a K&N Filter, and had over-oiled it. The excess oil got pulled off into the intake stream and coated the MAF, leading to incorrect readings and hence incorrect A/F ratio.
My 2000 ws6 was the exact same way









