Installed headers, runs worse, HELP!
So i put headers on the vet last night, now it runs like $hi7, wont rev past 4k nad stumbles to get there, now i have a pcmforless chip(tuned for removal of air and egr) that should be here tomorrow along with all the egr block off plates needed ot remove the egr crap. My question is with all the egr and air stuff being removed and no block off plates could this cause the stumbling? also throwing only code 26. Mind you this it racn perfectly for the first few weeks of ownership(just bought) and would destroy the tires in first gear, it did however one night just randomly start having a low rpm stumble and a slight loss in power, i was thinking it was probably a bad plug because it did have a bad 02.
Well last night while i was there I installed brand new NGK tr55s gapped @.35, and two new O2s along with some OBX LT's. Also yanked out all the EGR/AIR crap, i do however have two large holes in the rear of the intake where the EGR valve was since my block off plates didnt get here yesterday like i thought. So my question is did i make an existing problem that just randomly arose a week or so ago worse during the install, or is it possible i fixed one issue(the potentially fouled pkugs) and replace it with a worse issue in removing the EGR/AIR stuff?
Well last night while i was there I installed brand new NGK tr55s gapped @.35, and two new O2s along with some OBX LT's. Also yanked out all the EGR/AIR crap, i do however have two large holes in the rear of the intake where the EGR valve was since my block off plates didnt get here yesterday like i thought. So my question is did i make an existing problem that just randomly arose a week or so ago worse during the install, or is it possible i fixed one issue(the potentially fouled pkugs) and replace it with a worse issue in removing the EGR/AIR stuff?
Actually made typo egr valve is still their just all the plumbing that went to passenger manifold and into back of intake is gone, its left a nickle sized hole yet it doesn't appear to pull vacuum when cars running. So guess its a mystery problem and not that. also always have gapped my plugs on my lt1s at .35 never any issue. idk what the f is wrong with it. makes me sad






