cecil wednesday (8/10)?
#23
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Pretty much all loaded up...just need to grab a few tools from the garage and my ice for the intercooler
Depending on how things go, I may try my first few license upgrade passes if there are two A/ET license holders there tonight...
Depending on how things go, I may try my first few license upgrade passes if there are two A/ET license holders there tonight...
Last edited by Fireball; 08-10-2011 at 07:19 AM.
#27
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0 for 3 last night
first pass...1.39 60', blew the tires HARD at 100' out....car went completely sideways at 75mph
2nd pass...1.36 60'... had a sync loss with my crank sensor at top of first gear (aborted)...tightened up the gap some more...
3rd pass...1.33 60'...idiots at the track wasn't paying attention and let a truck roll down next to me after I started building boost. Had to back off and restart...most likely overheated the converter/trans and blew through 2nd gear bad
fugger is making some serious power now...hit 33psi...Ended up going 9.80 only in the gas for 300ft
first pass...1.39 60', blew the tires HARD at 100' out....car went completely sideways at 75mph
2nd pass...1.36 60'... had a sync loss with my crank sensor at top of first gear (aborted)...tightened up the gap some more...
3rd pass...1.33 60'...idiots at the track wasn't paying attention and let a truck roll down next to me after I started building boost. Had to back off and restart...most likely overheated the converter/trans and blew through 2nd gear bad
fugger is making some serious power now...hit 33psi...Ended up going 9.80 only in the gas for 300ft
Last edited by Fireball; 08-11-2011 at 06:03 AM.
#29
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we'll get it fixed up tomorrow
Last edited by Fireball; 08-11-2011 at 07:27 AM.
#30
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It was nice seeing the car go down the track again. The first pass scared the heck out of all of us. We heard tires screech, the turbo go into full boost quickly, and saw the bumper pointing at the wall. Thankfully Brian recovered.
I hope the trans issue is very minor and you are back on the road soon enough!
I hope the trans issue is very minor and you are back on the road soon enough!
#32
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Dont blame the track guys. I heard they make like 40.00 a night... You get what you pay for in terms of help...
0 for 3 last night
first pass...1.39 60', blew the tires HARD at 100' out....car went completely sideways at 75mph
2nd pass...1.36 60'... had a sync loss with my crank sensor at top of first gear (aborted)...tightened up the gap some more...
3rd pass...1.33 60'...idiots at the track wasn't paying attention and let a truck roll down next to me after I started building boost. Had to back off and restart...most likely overheated the converter/trans and blew through 2nd gear bad
fugger is making some serious power now...hit 33psi...Ended up going 9.80 only in the gas for 300ft
first pass...1.39 60', blew the tires HARD at 100' out....car went completely sideways at 75mph
2nd pass...1.36 60'... had a sync loss with my crank sensor at top of first gear (aborted)...tightened up the gap some more...
3rd pass...1.33 60'...idiots at the track wasn't paying attention and let a truck roll down next to me after I started building boost. Had to back off and restart...most likely overheated the converter/trans and blew through 2nd gear bad
fugger is making some serious power now...hit 33psi...Ended up going 9.80 only in the gas for 300ft
#34
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Dan you may apply I am sure they would love to have you... Matter of fact MIR just advertised help wanted.
#35
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I thought about doing it, doesn't seem like all that bad of a job i like being on the starting line. But then realized it's an hour and half away. If it was right around the corner, i'd apply.
Side note mike you guys heading to crapitol tomorrow?
Side note mike you guys heading to crapitol tomorrow?
#36
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I beleive we are... Hit up your wifey on FB to see if you guys were coming. Love ya Steve but still sad I missed the wifey losing her swim cover on the beach... You will have to share some photos...
#37
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first run (definately drove out of the groove...probably why it spun)
http://www.youtube.com/watch?v=M21M0TGNRfE
third run (blew through the shift and hit the rev limiter...pretty cool fireballs In the gas ~4seconds... and coasted to a 9.80
http://www.youtube.com/watch?v=mVIMfGSU_wo
http://www.youtube.com/watch?v=M21M0TGNRfE
third run (blew through the shift and hit the rev limiter...pretty cool fireballs In the gas ~4seconds... and coasted to a 9.80
http://www.youtube.com/watch?v=mVIMfGSU_wo
Last edited by Fireball; 08-11-2011 at 08:20 PM.
#39
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Pulled the glide out last night and taking to my trans guy today...
don't look too bad...normal amount of clutch in the pan. fluid was definately cooked. Front vent line that goes to a trans catch can was pinched, so the fluid actually found its way out the rear vent in the tail housing. Trans guy told me it had to be stupid hot for that to happen
didn't blow by the front seal at all
nonetheless...I'm adding a 2nd trans cooler. I currently have a Derale fan cooled cooler but will add a 2nd one that sits in my icewater tank
don't look too bad...normal amount of clutch in the pan. fluid was definately cooked. Front vent line that goes to a trans catch can was pinched, so the fluid actually found its way out the rear vent in the tail housing. Trans guy told me it had to be stupid hot for that to happen
didn't blow by the front seal at all
nonetheless...I'm adding a 2nd trans cooler. I currently have a Derale fan cooled cooler but will add a 2nd one that sits in my icewater tank