Strange problem here....
Here is what is going on.......
1. saw 15psi boost with same pully that only made 8-9 on other engine.No detonation or knock.
2. This cams power(224/230 581/592 114lsa) Peaked and tapered out at a slightly lower rpm than the stock cam
We talked about possible causes for this. It looks like the cam was installed incorrectly. Off a couple of teeth or somthing. Must have the valve timing all
screwed up. The high boost is an indication of a restriction, and since it didnt detonate it must be backing up in the manifold. I ended up leaving the truck with Allan to look into it. Hopefully it will be as easy as pulling the front cover and getting the cam set right. I know I have left my truck in very good hands
The engine is a stock bore 6.0. Only change when rebuilt was the cam and a set of diamond pistons. Everything else on the truck is the same as my 442rwhp dyno pull with a completely stock 6.0.

