Update: Help with pully removal? Problem.
UPDATE: Ok so I got the pully on and seated using a threaded rod M16 at 2.00 same as the bolt that came out. Anyway so I put the old GM bolt in and torqued it to the specs on my instruction sheet. The bolt went in easy didn't force it. So when I go to back it out for the new bolt it won't move. Finally got it out and it looks like this one in this thread. https://ls1tech.com/forums/generatio...cs-inside.html
What the hell happened? I didn't use the bolt to seat it as I have read many times not to. Am I screwed? Any suggestions?
Last edited by Breathing Fire; Dec 30, 2009 at 07:19 PM. Reason: New issue
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Back before I had any air tools I'd stand in the engine bay and jump on the breaker bar.
GET A THREADED ROD!!! With the same threads, some washeres and 2 Nuts.
Seating the rod to the bottom gives the most strength and stability and will not allow the bolt to be broken. I used McMaster for the rod but any place with the correct pitch and thread count will do the trick. I have seen countless guys strip the threads or break bolts off because they were lazy.






