The Car Is Alive Again!!
The car b4 cam swap dynoed 331/340 on a fresh recalibrated mustang dyno...
i posted this in anther post:
My speed shop called, they said that my Trans Am *MAY HAVE A BLOWN HEAD GASKET* the reason that they say is b/c there was very little coolant in the radiator, 20 oz. But when they drained the oil outta the motor it was crystal clear they said. Also in my oil catch can, the oil was like a milky color. i was thinking that there was water in the crankcase, i only drove the car for 20 miles when i checked it, water did not evaporate?? Another thing to note, before i put the ta in storage i did a coolant flush. now i am thinking that maybe there was some air pockets, and when they air pockets got out, it caused the coolant level to drop???? I never did check it again after i stored it , thought that it would be fine?? The shop said that there was a spot on the drivers side header coming the from what looked like the head but that could have been from when i washed the car with an undercarriage was, also when i washed the motor as well? i did wash the car with an under carriage was on 12/16/06...
Any ideas????? i think air pockets are the cause of this????????
let me know what you guys think?
Wonder what numbers i will make after the cam?? 228/232 .588/.595 110+4
Like it was said your rwhp will depend on other factors such as the intake and underdrive pulley.
jsut a cam swap with.
ASP pulleye, LS6 Oil Pump ported and shimmed and LS2 timing chain
Like it was said your rwhp will depend on other factors such as the intake and underdrive pulley.
Yup Mike is a good guy there. They had the car running yesterday. went to tune it today, and i did not start
he said either starter, battery or alt...WTF
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Vid to come with nice weather. and yes i lie to make sound clips
Hey Brad, the name is Jonas BTW... Soundclip will be soon
The car was running fine yesterday after the cam install. Went to tune it today and it did not crank. Either starter, battery or alt

Why me, it was fine beofre hand
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Hey Brad, the name is Jonas BTW... Soundclip will be soon
The car was running fine yesterday after the cam install. Went to tune it today and it did not crank. Either starter, battery or alt

Why me, it was fine beofre hand


i got a pulley, but when they were heat cycling the car, it was a high idle so there should be no charging problems. Lights i would say no, b/c after 10 mins they shut off.. maybe battery, it is the original batter from 2001/2002 when ever the car was built. and i know i had a hell of time starting it to deliver to the shop on monday. It was -9 out when i started it.. But it still started.. Think i coulda strained it???
But yea i have been doing so much research.. I want results too lol.... I did dyno 331/340.. thought it was it low. but ahh ok
anymroe ideas
anyways, first pull it made with a little tuinng was 402 RWHP A:F was at 12.8.. going to pick it up today.. they are not done tuning it yet....
Man i am stoked
No, mustang dyno
Brad...
pulled 405 RWHP with 375 RWTQ....
SAE corrected: 415 RWHP with 378 RWTQ
A:F was 12.8.. Need bigger injectors
from my mods in sig that is over 75+ HP My car took well to this cam
Still need to work on some tuning issues. Need to write a quick PM.. He told me so...
BRB Last edited by TORCHD 02 TA; Feb 7, 2007 at 09:14 PM.
so do you think that it is a battery? And what do you recommend to replace it? I have to check funds to see if i can get an optima red top, if not what is the other alternative????


