24x Le2 355 problems after 1st drive
As my wife would say: "THAT'S DISCRIMINATION!"
Looking forward to hearing how it turns out.
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FYI: Finally turned the key on my build, and the engine turned over, but no fuel.
A buddy of mine was in the shop when I got the Racetronix kit in and I let him install it... .
Another update...
Got a call from the shop. The car is now running on 4 cylinders. Luckily they found out why. Passenger side coil harness connection "on the main harness side" has some charring. Apparently when it was only running on 4 cylinders they could shake the harness connector and it would kick back into 8. Shop said they tried to fix it but it looks like I need to get a new connector. They said that with the poor connection it arched a little and damaged the connector. Now I'll have to wait till Monday to find the connections.
Got a call from the shop. The car is now running on 4 cylinders. Luckily they found out why. Passenger side coil harness connection "on the main harness side" has some charring. Apparently when it was only running on 4 cylinders they could shake the harness connector and it would kick back into 8. Shop said they tried to fix it but it looks like I need to get a new connector. They said that with the poor connection it arched a little and damaged the connector. Now I'll have to wait till Monday to find the connections.
Another update...
Got a call from the shop. The car is now running on 4 cylinders. Luckily they found out why. Passenger side coil harness connection "on the main harness side" has some charring. Apparently when it was only running on 4 cylinders they could shake the harness connector and it would kick back into 8. Shop said they tried to fix it but it looks like I need to get a new connector. They said that with the poor connection it arched a little and damaged the connector. Now I'll have to wait till Monday to find the connections.
Got a call from the shop. The car is now running on 4 cylinders. Luckily they found out why. Passenger side coil harness connection "on the main harness side" has some charring. Apparently when it was only running on 4 cylinders they could shake the harness connector and it would kick back into 8. Shop said they tried to fix it but it looks like I need to get a new connector. They said that with the poor connection it arched a little and damaged the connector. Now I'll have to wait till Monday to find the connections.
Update finally....I just got home with my car. I actually drove her home from the shop. Sure it was only 30 miles, but I haven't driven her in about a year. Still has some bugs to workout.
1st the transcooler I have is too small for my 3600. The shop told me that I needed a bigger cooler and it never got over 200 degrees, but they didn't drive it far. It got up to 240 degrees while I was driving so I pulled over and stopped at one of the stations I work at and let it cool. Drove home and got up to 240 again. So because the trans was running hot I never got on it to see what she would do.
2nd The car has also developed a squeal when turning left. I'm thinking it's a front wheel bearing but I'm not sure yet.
3rd The shop never tuned for the P0452 or the P0757. They both showed up a mile from my house.
4th They didn't recharge the AC.
5th unfortunately the guy that tuned it wasn't there today. He's the guy that has my dyno results and a video. That kinda frustrated me but it's not that big of a deal. I'd just like to see what kinda power she's making.
As far as I'm concerned, they're all little issues. The car is now running and that's progress.
1st the transcooler I have is too small for my 3600. The shop told me that I needed a bigger cooler and it never got over 200 degrees, but they didn't drive it far. It got up to 240 degrees while I was driving so I pulled over and stopped at one of the stations I work at and let it cool. Drove home and got up to 240 again. So because the trans was running hot I never got on it to see what she would do.
2nd The car has also developed a squeal when turning left. I'm thinking it's a front wheel bearing but I'm not sure yet.
3rd The shop never tuned for the P0452 or the P0757. They both showed up a mile from my house.
4th They didn't recharge the AC.
5th unfortunately the guy that tuned it wasn't there today. He's the guy that has my dyno results and a video. That kinda frustrated me but it's not that big of a deal. I'd just like to see what kinda power she's making.
As far as I'm concerned, they're all little issues. The car is now running and that's progress.






