383 hp loss
And pulling a motor rather than simply replacing exhaust gaskets KNOWN to be blown makes no sense at all.
IF in fact you are truly 'trying to get the car running'... I suggest you close your mouth and open your ears, because I PROMISE the combined knowledge you are blowing off in this thread alone, let alone the folks who read this and passed on trying to help because of your attitude, is far greater than the knowledge you believe you have, at least when it comes to LT1s.
I'm considering dropping my 94's engine to find a knock, probably due to a lifter, rather than pulling the intake under the cowl. if it turns out to have wiped a cam lobe, it'll be far easier to pull the cam while it's out.
While it's out: look CLOSELY for burns on the plug wires, the computer will NOT throw a code for misfire on OBD1 cars even if one plug is shorting completely. Read ALL the plugs, and keep track of which hole they came from. (Bad misfire MIGHT not be felt, it'll throw the A/F on all the other cylinders off, and cost buttloads of power.) If you do pull it apart, it's tempting to say throw rings and bearings in... but at the least pull the intake, check all lifters, and look CLOSELY at the cam lobes. BRIGHT light, and all the way around. Smell the oil; if it's way rich, the oil will stink, and it may well have washed down the rings.
motor was a 383 with 30k miles on it in a 94 camaro Z28 with 124k on the chassis
-1.6 RR
-3.75 stroke crank forged
-3.030 bore with forged pistons
-I beam forged rods
-stock ported heads
-CC306 cam
-700R4 with factory torque convertor
-factory driveline
-factory 10bolt
---**transmission went out and was in and out of the shop 6 times due to the transmission ******* up*** finally they got it on the 6th trans. still same tq convertor and they said it wasnt flushed or anything
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when my other friend bought it
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same setup and still ran 11.30s for a month
the car sat for a week or so. came back to take it out and ran good still. parked it and tried it the next day and it was gutless
now runs HIGH 13s to low 14s
reson being i thought possible torque convertor is the paint it bubbled and the fact it went through that many transmissions there has to be **** in it
now we have. NEW
-coil
-FPR
-MAF
-MAP
-TEMP sensors
-pan gasket
-timing cover gasket
-new oil ((NEEDED IT))
-new wires
-new plugs
-completely sealed exhaust
-new torque convertor
-new rearend
NEVER HAVE REPLACED OPTI. but doesnt throw codes. is there any way to check the opti
anythingelse i forgot i will add later. when the car is back together i will try to put a datamaster file on the net for anyone wanting to look at it.
All cylinders DO have spark, all spark plugs have been replaced and still look fine.
When you unplug #1 and #6 fuel injectors to test for a dead cylinder, the running of the engine DOES NOT CHANGE AT ALL. Making me believe that 1 and 6 are not firing. We tested the wiring with a noid light, and it was flashing. Injectors were replaced and nothing changed. Tested the plug wires for spark, they do spark.
Tested unplugging them again to check for dead cylinders, and sure enough they are dead. Unplugging #1 and #6 injectors does not effect how the engine runs, AT ALL. Unplugging any other injector and it surges and wants to die at idle.
FlashLCD33 - What are the plugs gapped @? And are you sure that the plugs are not internally fucked up. It could look fine and still not function properly. And when you say fine, whats that meen? If the cyl is not firing, surely there is some indication of something, fuel, oil, coolant, burning clean, SOMETHING. And is the fuel getting into the cyl? Did you check the flow of the inj?
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