Forced Induction Superchargers | Turbochargers | Intercoolers

370/Ls3 F1a dyno results

Thread Tools
 
Search this Thread
 
Old 04-15-2015, 08:38 PM
  #1  
TECH Resident
Thread Starter
iTrader: (12)
 
speedfreak2685's Avatar
 
Join Date: Jul 2005
Posts: 765
Likes: 0
Received 0 Likes on 0 Posts

Default 370/Ls3 F1a dyno results

1999 Camaro
370" iron block with Callies Compstar rods, Weisco -3.2cc pistons 10.6:1 I believe
stock crank
Ls7 lifters, custom grind cam from Tick Performance
stock Ls3 heads decked .035 with ls9 gaskets
F1a head unit with no filter, just a homemade screen
4.13" blower, 8.65" CBR crank pulley, Aster bracket
ATI ballancer
4" procharger front mount
1 7/8" TSP longtubes, TSP true duals straight piped
Ls3 intake, 90mm TB
9" rear with 3.89 gear
M6 with Monster lt1-sc twin disk

Fuel system
twin 450 pump squash setup
PTFE -8 line, Holly rails
1600cc injectors
E85

937/842

Motor lost oil pressure right after the dyno while street tuning it so the motor is coming back out. Pretty much sucks but is what it is. Its very evident by looking at the oil filter that it wiped out a bearing/bearings somewhere. I'm not sure if the crank flexed or something and messed up main or what. It had about 600 miles on it and 4 oil changes with no wot pulls up until this so im leaning towards crank but who knows till its apart. I'm going to go ahead and put a forged crank in it and likely put a set of thicker deck aftermarket heads and shoot for close to the 1000 mark. Just not sure which ones to go with yet. It was picking up big gains from every degree of timing added but had to stop because it started pushing water. I know Ls3 heads are kinda known for that and im sure cutting them .035 just made matters worse.

Name:  0DF2A4E1-9A99-4CB1-A04E-2C473EFE1E98_zpsbytt9syd.jpg
Views: 668
Size:  91.6 KB

Name:  9453EC3D-A5EC-4A0B-A9C8-C0917D44B5EC_zps6dcpsdjq.jpg
Views: 467
Size:  83.1 KB

Name:  5DA3D0A5-FBEB-4686-B8D9-DF97E5AA9466_zpsjonj2um2.jpg
Views: 425
Size:  228.6 KB
Old 04-15-2015, 08:42 PM
  #2  
TECH Enthusiast
iTrader: (52)
 
HISS's Avatar
 
Join Date: Jul 2013
Location: Corpus Christi Texas
Posts: 580
Likes: 0
Received 1 Like on 1 Post
Default

That thing is making some steam literally and figuratively.
Old 04-15-2015, 08:49 PM
  #3  
TECH Resident
Thread Starter
iTrader: (12)
 
speedfreak2685's Avatar
 
Join Date: Jul 2005
Posts: 765
Likes: 0
Received 0 Likes on 0 Posts

Default

Originally Posted by HISS
That thing is making some steam literally and figuratively.
Im picking up what your putting down there
Old 04-15-2015, 08:56 PM
  #4  
TECH Enthusiast
iTrader: (52)
 
HISS's Avatar
 
Join Date: Jul 2013
Location: Corpus Christi Texas
Posts: 580
Likes: 0
Received 1 Like on 1 Post
Default

Originally Posted by speedfreak2685
Im picking up what your putting down there
Lol. It's a badass car.
Old 04-15-2015, 09:43 PM
  #5  
TECH Resident
Thread Starter
iTrader: (12)
 
speedfreak2685's Avatar
 
Join Date: Jul 2005
Posts: 765
Likes: 0
Received 0 Likes on 0 Posts

Default

Originally Posted by HISS
Lol. It's a badass car.
Thanks man. Hate I didn't get to enjoy it before it had to be torn down again.
Old 04-15-2015, 10:00 PM
  #6  
TECH Resident
iTrader: (28)
 
007FJ's Avatar
 
Join Date: May 2014
Location: Texas Gulf Coast
Posts: 859
Received 62 Likes on 54 Posts
Default

If mine will put down over 800 on a similar built F1C 93/Meth with the air filter, I will be happy. Almost have it back together.

Your results are most excellent. Right up to that oil problem. The thinner deck heads have got to go. I have AFR 225's. Jason told me he and Chuck picked them to hold the deck down as much as anything flow related.

How much boost was it pushing?
Old 04-15-2015, 10:10 PM
  #7  
TECH Enthusiast
iTrader: (52)
 
HISS's Avatar
 
Join Date: Jul 2013
Location: Corpus Christi Texas
Posts: 580
Likes: 0
Received 1 Like on 1 Post
Default

Originally Posted by speedfreak2685
Thanks man. Hate I didn't get to enjoy it before it had to be torn down again.
Just think.....if it made that power hurt it'll make more happy.
Old 04-15-2015, 10:23 PM
  #8  
TECH Resident
Thread Starter
iTrader: (12)
 
speedfreak2685's Avatar
 
Join Date: Jul 2005
Posts: 765
Likes: 0
Received 0 Likes on 0 Posts

Default

Originally Posted by 007FJ
If mine will put down over 800 on a similar built F1C 93/Meth with the air filter, I will be happy. Almost have it back together.

Your results are most excellent. Right up to that oil problem. The thinner deck heads have got to go. I have AFR 225's. Jason told me he and Chuck picked them to hold the deck down as much as anything flow related.

How much boost was it pushing?
Yea I'm going to likely go with PRC or trick flows.

20-21#. Had a little belt slip/walk which I addressed when I got it home from the dyno so maybe it will make another pound now but who knows.
Old 04-15-2015, 10:23 PM
  #9  
TECH Resident
Thread Starter
iTrader: (12)
 
speedfreak2685's Avatar
 
Join Date: Jul 2005
Posts: 765
Likes: 0
Received 0 Likes on 0 Posts

Default

Originally Posted by HISS
Just think.....if it made that power hurt it'll make more happy.
I like the way you think
Old 04-15-2015, 10:41 PM
  #10  
TECH Resident
iTrader: (28)
 
007FJ's Avatar
 
Join Date: May 2014
Location: Texas Gulf Coast
Posts: 859
Received 62 Likes on 54 Posts
Default

Did you have a filter on it?
Old 04-15-2015, 10:44 PM
  #11  
TECH Resident
iTrader: (28)
 
007FJ's Avatar
 
Join Date: May 2014
Location: Texas Gulf Coast
Posts: 859
Received 62 Likes on 54 Posts
Default

Between my vacuum pump, AC, Alky Control, Line Lock, and Dual Intercooler System your engine compartment looks naked!
Old 04-15-2015, 10:47 PM
  #12  
8 Second Club
iTrader: (19)
 
oscs's Avatar
 
Join Date: Jan 2013
Location: Cypress, TX
Posts: 3,903
Likes: 0
Received 4 Likes on 4 Posts
Default

Damn that sucks. My LS3 heads have seen 26psi on my 370 without any issues so far.
Old 04-15-2015, 11:49 PM
  #13  
10 Second Club
iTrader: (14)
 
Detoxx03's Avatar
 
Join Date: Jan 2007
Location: Woodward Avenue
Posts: 7,336
Received 72 Likes on 37 Posts

Default

Hate that that happened but it made some nice power. I'm sure it will be back stronger and better. What was the IDC?
Old 04-16-2015, 12:37 AM
  #14  
8 Second Truck Club
iTrader: (32)
 
Blown06's Avatar
 
Join Date: Apr 2006
Posts: 5,181
Likes: 0
Received 8 Likes on 8 Posts

Default

Story of my life

it kept going faster and faster and faster and loosing more and more and more water
Old 04-16-2015, 06:15 AM
  #15  
TECH Veteran
iTrader: (7)
 
forcd ind's Avatar
 
Join Date: Sep 2007
Location: woodbine, md
Posts: 4,116
Received 230 Likes on 162 Posts

Default

Well, at least you found the weak points-bummer though
Old 04-16-2015, 07:17 AM
  #16  
TECH Resident
Thread Starter
iTrader: (12)
 
speedfreak2685's Avatar
 
Join Date: Jul 2005
Posts: 765
Likes: 0
Received 0 Likes on 0 Posts

Default

Originally Posted by 007FJ
Did you have a filter on it?
Nope, just a screen to keep anything large out of it.
Old 04-16-2015, 07:18 AM
  #17  
TECH Resident
Thread Starter
iTrader: (12)
 
speedfreak2685's Avatar
 
Join Date: Jul 2005
Posts: 765
Likes: 0
Received 0 Likes on 0 Posts

Default

Originally Posted by 007FJ
Between my vacuum pump, AC, Alky Control, Line Lock, and Dual Intercooler System your engine compartment looks naked!
Ac is going back on the car. Just haven't put the lines back on since the swap.
Old 04-16-2015, 07:19 AM
  #18  
TECH Resident
Thread Starter
iTrader: (12)
 
speedfreak2685's Avatar
 
Join Date: Jul 2005
Posts: 765
Likes: 0
Received 0 Likes on 0 Posts

Default

Originally Posted by oscs
Damn that sucks. My LS3 heads have seen 26psi on my 370 without any issues so far.
Dang that's awesome. I'm sure mine being cut .035 isn't helping my cause either.
Old 04-16-2015, 07:21 AM
  #19  
TECH Resident
Thread Starter
iTrader: (12)
 
speedfreak2685's Avatar
 
Join Date: Jul 2005
Posts: 765
Likes: 0
Received 0 Likes on 0 Posts

Default

Originally Posted by Detoxx03
Hate that that happened but it made some nice power. I'm sure it will be back stronger and better. What was the IDC?
If I remember correctly around 90% at like a 50# base. I started with fic127 that they swore would be plenty for 1000. The first pull the car made like 860 and they were already at 130% with a 58# base pressure.
Old 04-16-2015, 07:23 AM
  #20  
TECH Resident
Thread Starter
iTrader: (12)
 
speedfreak2685's Avatar
 
Join Date: Jul 2005
Posts: 765
Likes: 0
Received 0 Likes on 0 Posts

Default

Any input on head choices is welcomed. I need to be around a 64cc to keep compression where it's at now I believe. Also I believe I'm going to go with a k1 stock stroke crank.


Quick Reply: 370/Ls3 F1a dyno results



All times are GMT -5. The time now is 08:35 PM.