%#&! (not happy)
#1
Staging Lane
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%#&! (not happy)
It looks like the TSP motor has gone bye bye... I'm a little disappointed, Well actually I'm alot disappointed. I haven't even got 5,000 miles out of it yet . I was deployed all last year, came home and put about 2000 easy miles on her (no racing or track time) and this morning when I go to start it, it immediately started knocking so I shut her down and coolant started spewing somewhere out of the block on the passenger side of the oil pan. I only got a chance to pull the passenger side valve cover before the toe rig showed up. The springs looked amazing, everything was tight. I couldn't find the source of the leak while the car was in my driveway. I have no tools here, just basic hand tools. Hopefully the shop will figure out what the deal is. So, anybody in the Tampa bay area wanna help with a pending motor swap?!!
Its extremely frustrating because she was running so well up until this morning. Oh well, I guess its life. I'll find out more tonight on the extent of the damage. I'm guessing maybe since its been 2 or 3 days since it was last started, its possible that a small head gasket leak filled up a cylinder and caused this to happen? Its killing me not knowing officially. Guess I'll have to wait.
Its extremely frustrating because she was running so well up until this morning. Oh well, I guess its life. I'll find out more tonight on the extent of the damage. I'm guessing maybe since its been 2 or 3 days since it was last started, its possible that a small head gasket leak filled up a cylinder and caused this to happen? Its killing me not knowing officially. Guess I'll have to wait.
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Staging Lane
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I doubt it's anything TSP did. I built the top end, and the oiling parts. You guys know how that goes. It seems that the number 4 cylinder was the culprit. Hydrolock is a bitch. It put a 4 inch crack in the block leaking coolant into the oiling system and all over the ground. I'm just not sure why and where and how I got the leak. I mean, the car was running flawless 4 days ago. I'm not running FI or anything crazy. It just sucks. I think I'm going to go ahead and let the shop take care of it. I've never let anybody touch that car except for me, but I think i've had it. I feel like its my fault. I guess if I let someone else do it and it fails I can blame them lol.
It looks like we will be able to reuse most of the parts, minus the block and at least 1 of the pistons/rods, so thats good. We'll know more tomorrow in terms of that. I'll try to post pics when I get them. Anybody have a better option than a rebuild? Its going to cost roughly 12-1600 to machine a new block and fit th eold parts in there. I'm open to suggestions.
It looks like we will be able to reuse most of the parts, minus the block and at least 1 of the pistons/rods, so thats good. We'll know more tomorrow in terms of that. I'll try to post pics when I get them. Anybody have a better option than a rebuild? Its going to cost roughly 12-1600 to machine a new block and fit th eold parts in there. I'm open to suggestions.
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#8
Staging Lane
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Oddly, it poured here yesterday... But I never drove the car. Its pretty tight and everything on top was buttoned down. So, I doubt that was it. It sat for a couple days. I think the only explanation is a leaky head gasket.
#10
Staging Lane
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Stuck open? It was Instantaneous with initial start up. As soon as it turned over once, I knew something was seriously wrong. So, I doubt it was an injector. Like I said, its NA so i'm not pushing THAT much fuel.
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I say by a Iron 6.0 from scoggin dicky for 700 bucks and use the rotating assembly that you all ready have should be a nice 370 ci. I think the price u pay for machining would offset the price for the 6.0 new. Oh and everything off your motor will button right up except one altanator bolt.
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Staging Lane
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I would like to do the 370, I'm just not too sure how soon he could get that block. Its my daily driver and I have to be back in TN by next Wed. He's got an alum. 6.0 at the shop that we could drop in, but I'm not sure on the details of the motor at this time. I will know more about options once we tear into the block today.
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I'll have them look at the injectors. Those were put in a couple months ago when I had the car re-tuned by a shop here in Tampa. I suppose that is more logical than the head gasket theory.... Interresting
I would like to do the 370, I'm just not too sure how soon he could get that block. Its my daily driver and I have to be back in TN by next Wed. He's got an alum. 6.0 at the shop that we could drop in, but I'm not sure on the details of the motor at this time. I will know more about options once we tear into the block today.
I would like to do the 370, I'm just not too sure how soon he could get that block. Its my daily driver and I have to be back in TN by next Wed. He's got an alum. 6.0 at the shop that we could drop in, but I'm not sure on the details of the motor at this time. I will know more about options once we tear into the block today.
I would DEFINITELY want to find the root cause of your problem before throwing another engine in there and having it happen again..
#20
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just wondering, what head gasket did you use?
Not sure. Whichever ones TSP sent with the entire package. I think just the stock style GM's. They were not MLS's.
I just came back from the shop, looks like (due to time constraints) I will have to go with a slightly used (stock) 6.0L LQ4 and just bolt on the rest of my crap. Not too crazy about that, but I do not have many other options since I need the vehicle by Wednessday to get back to Ft. Campbell. The builder will back the motor for 12,000 miles/1 year.
It sucks, I was this close to saying screw it, and getting the iron 408.... But I really need the car by next week, and it would have been close to 3 G's more with a three week wait. The wife would have supported it, but I would have felt like an *** pouring another 6 grand into the car after last years fiasco. Anyway, I will have new numbers next week (yay...).
We are going to have the injectors flow tested/matched. The heads will have a clean up pass at least, possibly milled a tad more to get closer to 11:1. All in all, everything should work out great. Just a bummer because the old set up was really running strong, and just barely broke in!! I'm getting upset again just thinking about it. I'll keep y'all posted...
-Z
Not sure. Whichever ones TSP sent with the entire package. I think just the stock style GM's. They were not MLS's.
I just came back from the shop, looks like (due to time constraints) I will have to go with a slightly used (stock) 6.0L LQ4 and just bolt on the rest of my crap. Not too crazy about that, but I do not have many other options since I need the vehicle by Wednessday to get back to Ft. Campbell. The builder will back the motor for 12,000 miles/1 year.
It sucks, I was this close to saying screw it, and getting the iron 408.... But I really need the car by next week, and it would have been close to 3 G's more with a three week wait. The wife would have supported it, but I would have felt like an *** pouring another 6 grand into the car after last years fiasco. Anyway, I will have new numbers next week (yay...).
We are going to have the injectors flow tested/matched. The heads will have a clean up pass at least, possibly milled a tad more to get closer to 11:1. All in all, everything should work out great. Just a bummer because the old set up was really running strong, and just barely broke in!! I'm getting upset again just thinking about it. I'll keep y'all posted...
-Z