Trans went out
You may want to add some UMI Performance rear lower control arms part # 4015-B. these will help eliminate your wheel hop. While you’re in the trans another good idea would be to tame down that 1-2 shift.
1. Line pressure is too high. This can be caused by a defective engine sensor, an aggressive tune or a defective EPC (Pressure Control Solenoid).
2. Too tight of a 1-2 accumulator due to an aggressive shift kit. Never use the B&M shift kit as it disables the 1-2 accumulator completely. Generally no more than one washer should be used with the Transgo HD2 shift kit.
3. Other problem in the 1-2 accumulator such as a broken spring, cracked piston or worn bore. Always rebuild with an aluminum piston; throw any plastic piston away. If the Transgo HD2 kit's 1-2 springs are NOT used, the Sonnax Pinless piston is an excellent and suggested replacement.
Make sure your rebuilder uses the best BW HD dual-cage sprag. As mentioned, the Sonnax HD 2-3 shift valve will reduce the load on your sprag if you race in [D3]. Reminder - if you don't have that valve, you should race in [OD]. This thread might help you understand things better:
https://ls1tech.com/forums/automatic...ure-flare.html
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