Mustang notch LS build
Here's the car the day I got it.
Last edited by Lsxnafox; Jan 6, 2017 at 11:47 AM.


Last edited by Lsxnafox; Jan 6, 2017 at 11:47 AM.
The motor went in easy with a aje k member. At the time I was planing on doing a turbo setup so I put some v bands on the stock manifolds flipped forward. I ran the exhaust out in front of the tire for the time being so I could atleast fire up the motor and drive it around a bit. Used a Camaro shifter and just plugged the big hole where the stock shifter would go. Mustang tranny cross member worked fine just moved it back a bit.








Last edited by Lsxnafox; Jan 6, 2017 at 04:19 PM.
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The car sat for about a week, went out to fire it and it wouldn't start. Seemed as if the starter was on its way out. Seemed like it was getting caught on the flywheel and getting stuck. After a few tries it finally fire up. But now the motor had a bad knock. I couldn't believe it, when I last drove it it was fine now the motor was knocking. Pulled the motor and discovered this.

Yep, that's a bent gen4 rod. The noise was coming from the small end hitting the piston skirt.
And it gets worse. I had a spare motor laying around. A 6.0 lq4 I was planing on building into a 408. I decided to just throw it in so I could get back on track with the build. Once the motor was in and running I noticed there was coolant leaking from around the heads. At this point I figured a blown head gasket must be the problem. So when I went to remove the heads discovered all the head bolts werent TQ down. I think who ever I got it from pulled the heads to inspect the motor and didn't bother telling me.
Pulled the heads had them rebuilt and slapped it back together.

After a few weeks many sleepless nights I got back to work on the car.
It was now mid October the car was back up and running. Still on the to do list was fuel system and exhaust. Things just get plain embarrassing at this point. Maybe because of everything going on or for what ever reason I can't explain it I didn't bother to track down what caused the initial knock in the motor before replacing it with the 6.0. Well it happened again under the same conditions. It was running fine, let it sit for a few days went to fire it up and same thing. Starter got hung up. Finally fired it up with the same knocking are the prior motor. Very discouraging at this point.

As I suspected, after pulling the motor again!!! Bent rod same location are the prior one. Long story short and I'm sure many of you have figured I had an injector stuck open. As the car sat for several days fuel leaked down into the combustion chamber. Yep, hydrolocked causing the rod to bend.
If things couldn't get worse, what was supposed to be a simple task of cutting a small tab on the transmission shifter cable bracket attached to the tranny. I ended up almost cutting my thumb off. The cutting wheel on the grinder got hung up and walked right into my thumb nearly cutting it off.
Took 4 stiches.
[URL=http://s650.photobucket.com/user/franks03cobra/media/Mobile%20Uploads/IMG_20160901_130159394_HDR_1.jpg.html]

Took break from working on the car and shaved a truck intake.
Last edited by Lsxnafox; Jan 7, 2017 at 12:20 PM.
With all the setbacks I decided not to go turbo for the time being. I figured building a turbo kit was going to take even more time and now with two babies getting time to work on the car was hard. I got some LS swap headers from eBay and had the exhaust built. I also finished up the fuel system.
I used a new fuel hat that has 6an hose fittings really impressed with it and a walbro 450lph pump for e85.
Last edited by Lsxnafox; Jan 7, 2017 at 08:56 AM.
Cleaned up the interior.
E85 looks really good around here for being winter fuel.
Here's some video. Enjoy

Last edited by Lsxnafox; Jan 7, 2017 at 10:02 AM.
http://www.promracing.com/fuel-suppl...-mustangs.html


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