Conversions & Swaps LSX Engines in Non-LSX Vehicles
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1978 Aerocoupe Caprice: 5.3 / 4L60E

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Old 07-29-2018, 12:58 PM
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fyi on the power steering pump, the bottom fitting is metric thread and rather than use adapter fittings, i have been able to swap it with one from the older power steering pump and reuse the stock lines. might check this if you still have the old pump. and just make sure the o-ring that seals the fitting to the pump is in decent shape
you're making good progress
Old 07-29-2018, 08:51 PM
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350SS, thank you for the suggestion. I still have the old engine in the driveway so I got the old lines off of it and they bolted right up and fit perfectly. Man I can say thanks enough that just saved me a lot of time and effort!
Old 07-29-2018, 09:58 PM
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good deal....did you have to swap the fitting for the lines to work? i think the new one is metric bulb with an o-ring and the older stuff is a typical sae inverted flare...or did the stock line already have the metric fitting? just curious
Old 07-29-2018, 10:08 PM
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I didn't check the type of inlet inside the fuel pump fitting. I just tried the line and since it threaded on I thought I was good. I was afraid it was too easy. I can't barely see the fitting in the picture I listed above. How would I be able to visually tell the difference, just in case the O-ring is missing, because when I got the new 5.3 pump there was no line attached to it.
Old 07-30-2018, 12:37 PM
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i guess it depends on what the pressure line for the caprice looks like first off

inverted flare


gm metric with o-ring


you can swap these from one pump to the other if you need to keep the stock line


or you can use one of these adapter fittings to go from inverted flare to gm metric if needed


sorry for the huge pics...not sure how to resize these when uploading from a link...let me know if i'm shitting up your thread and i'll delete
Old 07-30-2018, 06:21 PM
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OK, I see. Thanks for the pics. I should be able to swap the fitting that screws into the body of each pump and then use my original line. That's the path I'm going to try to go with. Would it be as simple as just swapping one fitting for the other?
Old 07-30-2018, 06:59 PM
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that's what i was able to do on my nova...just check that o-ring in the third pic

fyi they also make adapters on the steering box fitting depending on what way you want to go
Old 07-30-2018, 08:14 PM
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I have some generic, green 0-rings. If the one I have is bad would one of those work for this application.. of course if the size is the same ?
Old 07-30-2018, 11:19 PM
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not sure on that one i'm sure any parts store would have something you could use ... probably needs to be rated for hydraulic or transmission fluid .. it will probably be fine, just thought you might as well check while you have it apart
Old 07-31-2018, 07:42 PM
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I swapped the old fitting into the new pump. I'll post pictures later. They were the same except for the inside where the hoses sealed. After installing the old in the new pump everything bolted right up.
Old 07-31-2018, 07:58 PM
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nice
Old 08-05-2018, 05:17 PM
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Here are the pictures of the Holley A/C bracket with Sanden 508 fully installed, minus the belt.










I wasn't exactly sure what to do about plumbing the power steering and then someone on the forums mentioned that the original lines should fit. I pulled the original lines off of the old engine and they not only threaded into the hole but they also lined up perfectly. Apparently the new pump is almost exactly in the same location as the old pump.


There is a 3rd line on the 2004 power steering pump that was originally used as a return line for the hydraboost brake system on the donor Avalanche. I'll crimp this line off and seal it.


I later found out that even though the old Caprice power steering line threaded into the back of the 2004 power steering pump, the new and old lines have different styles of fitting and they have different fittings internally in the back of the pump and that would not allow for a good seal. There were several options here and companies make adapters to fit the old hose to the new hose, but since I have the old pump I was able to swap the fittings in the back of the pumps that the power steering lines threads into. I pulled the fitting out of the old motor.




They look identical from the outside. The 2004 fitting is on the left and the original fitting is on the right.







however inside is a different story. The 2004 fitting is on the left, the original fitting is on the right.





After installing the old pump fitting in the back of the new pump the lines fit perfectly and bolted up just fine. That was a relief.


I finally prepared the dining room table for operation of the wiring harness. Funny enough, these sheets I'm using were actually used at a funeral home for covering embalmed bodies, brown blood stains and all, so this isn't the worst operation they've seen.




Here's the harness splayed out.







I started removing the loom and black tape.





And spaghetti went everywhere. I'm a bit overwhelmed here as I really don't fully understand what I'm doing. I'm just trying to take it one small step at a time.


I started back to work on the new gas pedal. I got the holes drilled in the mounting plate to attach it to the firewall. There were many different ways to accomplish what I needed to do. While I was at work I would design this in my head and then piece together the parts a little at a time.




I marked a plumb line on the plate while it was mounted in the car so I could align the pedal assembly straight.





One thing that made the mounting difficult was avoiding interference with all of the bolts coming through the plate while still getting the new pedal positioned properly.




I had to drill a hole in the pedal assembly with the hand drill because it wouldn't fit in the drill press.





This shows how the bolts were positioned so the pedal could mount flat without interference. My original plan was to use spacers between the pedal and the plate but I found this didn't give the the stability I wanted.


I also didn't want anything sticking out of the back of the plate between it and the firewall. The new pedal had two mounting holes, one on the bottom and one on the top, shown here.









I decided to countersink the bolts so they would sit flush with the back of the plate.





I was able to use the drill press to drill to drill the right depth without going too far. The 1/4 inch steel gave me enough material to achieve this.









Everything mounted up as planned.







And there was no interference with the pedal travel.







The silver bolts will be on the outside of the firewall when the assembly is mounted.




Old 08-05-2018, 05:18 PM
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Then it was time to relocate the pedal. I made this jig to help me put the new pedal in the right place.







I mounted the original assembly to the jig and marked where the pedal sat.







I used a drywall screw through the cardboard to locate the depth and height of the top of the pedal,





I mounted the assembly so that the bottom of the pedal aligned at the cardboard and I then marked that location on the cardboard.


Since the new pedal assembly will use the original holes I was able to mount the new pedal assembly to the same jig and reference the marked position of the old pedal. I drew a line on the new pedal arm for the cut.




And I chopped it off with my dwindling supply of cutting wheels.





I wanted to keep the original pedal. The new pedal arm would not mount to the original pedal so I had to cut the original pedal arm and mate it to the new pedal arm. With the new pedal assembly mounted on the jig I was able to locate where the pedal should be and begin to work from there.


For the entire build of the car so far, this was by far the most frustrating process yet. What seems like a quick and easy process in pictures actually equates to several hours of test fits and failed ideas and bruised fingers pushing the now stubby pedal arm down with no leverage. I did take the spring off. The electronics required a special socket to remove, so I was not able to take this apart. Because of the shape of the original pedal and the way it swiveled on the arm there were certain angles which could not be modified. Because of this, no matter in what position I put the pedal it would make contact when the arm would be mashed down fully. As I stated, I literally worked on this for hours trying to get the pedal to reside in it's original location without making contact when the pedal would be pushed to the floor.


I wanted to keep the welding on the new pedal arm to a minimal to keep the heat away from the electronics. Because of this, I didn't want to cut the arm too short and then have to reweld material back on if it wasn't absolutely necessary. As a result I went through several iterations of cuts to the original pedal arm, each time cutting a little bit more at a slightly different angle until I finally found one that was as close as could be achieved. I finally reached a point where I knew this was as good as it was going to get and I would have to make this it and deal with whatever else later. I welded a plate to the original arm with wet rags and vise grips used as heat sinks attached to the arm to protect the electronics on the assembly.


I then used the pedal and arm to locate where the new arm should be welded. It wasn't very pretty, but it's on there. Again, I wanted to keep the welding and grinding down to a bare minimum.




The position isn't exact but after a lot of playing with options I was able to get it relatively close.







The pedal arm did end up with some interference, but it wasn't too bad compared to the previous versions.





I marked the areas and ended up cutting off the bottom of the mounting plate and using a round file to cut a relief in the bottom of the pedal assembly and taking some length off the bolt.




At long last the piece was ready for primer and paint. This simple piece of steel took many hours just to get to this point.







The finished assembly, after paint, bolted together.










Start to finish, I probably have 16-20 hours in this assembly. Even though it looks pretty straight forward the placement of all of the pieces was so critical that finding a way to make all the parts work together in the right location was very time consuming to figure out. I understand it would have been much simpler to drill new holes in the firewall and put the pedal where it needed to be, but that's not how I wanted the finished product to be and one great thing about a project like this is you can do it however you want.




Here's the end result.







It seems to work well and allows full travel of the pedal with no interference, and I get to keep my original pedal.





The new radiator came in and fortunately even though it has a transmission cooler built in it is the same exterior depth as the radiator I returned so I was able to reuse the mounts I had previously made without modification. I glued some rubber inside the mounts and put some weight on them until it dried.




I flushed the heater core using this attachment for a garden hose I made a few years ago.







I finished up by running the heater hoses.


Old 08-05-2018, 07:52 PM
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nice progress. thanks for continuing to document and take pics...that's what used to make this forum great

might want to hold off on crimping that extra inlet on the ps tank...hydroboost brakes would be an awesome upgrade esp with a heavy car...can be had cheap out of late 90's early 2000's astro vans iirc. if you need a way to cap it a short piece of ps hose with a bolt in the end with a couple clamps works great
Old 08-05-2018, 10:44 PM
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Thanks. I wasn't sure if anyone was actually reading this anymore, but the forum has been so helpful for me I thought that it might help someone in the future.

I really don't know anything about hydraboost other than I assume it uses power steering fluid to assist the power brakes rather than vacuum. What are the pros and cons of that system?
Old 08-06-2018, 12:05 AM
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just a different way of providing power assist to the brakes and sometimes helpful in a system with low manifold vacuum or a heavy vehicle to require less pedal effort during braking. some say there is less modulation or pedal feel with them but i'm sure that could be adjusted. i think the main thing is less effort required to apply the brakes hard to get the car stopped but then again probably easier to lock them up which is where the modulation thing probably comes in.
Old 08-06-2018, 01:13 AM
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Subscribed. This is awesome! I have an 85 C10 and even though I went dbc. I had a different problem with the same style throttle pedal. I took the easy route and ordered a lokar billet pedal haha. I also took a look at the BRP kit, too much money for as much work as you had to put in. Keep up the good work! Many don’t understand the many hours it takes to make some of the small things go together.
Old 08-07-2018, 10:17 AM
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Nice work on the pedal! You won't be able to see the upper portion of the adapter, and as long as it works reliably, that's all that matters. Run it!
Old 08-11-2018, 11:55 PM
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Not a lot to show for a whole days work. I did take part of the day to gather and store all the extra parts in the barn loft, which will allow me to get the trailer out of the driveway, which will allow me to move the car closer to the garage, which will mean a little bit more shade during the day. Upon some advice I ended up ordering a condenser for a 1996 Caprice. It was a much better option than the universal condenser I was previously considering. This condenser already has the hardlines run in the correct location. This unit was a bit shorter in height than the previous unit. I was able to reuse the original rubber mounting cushions. I had to relocate the upper driver side mount toward the fender. Because this area is boxed I had to drill a hole and use a self tapping screw. It took quite a long time getting the exact combination of location and extra rubber correct. In the end it mounted tight and secure.










After a lot of trial and error I ended up marking and putting the lower radiator mounts on the radiator and then installing them together. As you can see below the condenser lines fit just right. I still haven't figured out a good solution for the upper mount. I can't find a piece of steel the right size to make something and I cannot find a metal break. I also cut a piece of heater core hose as a cushion between the core support and the radiator, just in case.


The PCM mount came in while I was working. I was hoping to mount the PCM tucked away and hidden in this location, but after test fitting it I realized that this option isn't going to work. It would also cause an extensive amount of modification to the wiring harness.


This leaves me with a lot of less desirable options for locations of the PCM. This seems to be the best option so far for several reasons, but I'm not sure how I feel about it being this close to the radiator.


The radiator and condenser have a gap of a little over an inch, which is more than ideal, but it is as close as I can get them and seems to be close to the original distance. I will need to add some air dams to keep the air going through the condenser.


I took the gear selector fork off of the old 350 turbo transmission and it fit on the 4L60E. At first it seemed certain it wasn't going to fit but after a lot of coaxing it finally came together. I'll have to remove it one more time to install the neutral safety switch when it comes in.


I finally got the BRP transmission crossmember fully mounted. I continually regret purchasing this kit. The crossmember kit is essentially a universal kit. The bolts in the center transmission mount were too short. When I contacted the company they told me to just go buy longer bolts. The transmission crossmember requires an extra bracket on the driver side. The instructions with the kit, which must be downloaded in a PDF from the internet, do not include this extra bracket and show pictures of a different crossmember that is longer and do not require the extra piece. When I looked up instructions for different types of cars it does include this extra bracket. Also, the bracket does not fit the car as instructed. Given all of this I began to suspect I was sent the wrong kit. I contact the company again and they informed me that this correct and to ignore the crossmember in the directions. Also, the bracket shown requires holes to be drilled in the frame, but it mounts on top of the frame. This means there's no way to located or mark where the holes should be. I ended up having to hold my finger in the hole on top of the frame where the bracket will mount and try to match that location with my other finger on the bottom of the frame. I've had three people look at the instructions and try to understand how this piece should be installed and none of them can figure it out. I eventually just took the piece, ignored the instructions, and found a way to make it fit.


I then disassembled the extra bracket and used it to help locate the second bracket hole by holding it under the frame. I basically used a punch to draw an arc indicating the possible locations for the second hole and then reinstalled everything correctly, held my finger over the hole and guessed the best location. Again, the reason I ordered this kit is that is appeared, because of the description and instructions which I viewed ahead of time, that it would require no drilling or modification.




At long last, everything was bolted up and tightened down.







There are quite a few pieces on order that I'm waiting to come in. This thing is starting to look like a driveable car.







Old 08-15-2018, 12:02 PM
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awesome build man glad to see im not the only aero fan around here with an ls swap! if you do it again the holley g body swap plate work just fine for factory placement


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