New best with a scare
60'- 1.37 spun and shook the tires a little
330'- 3.73
1/8 ET- 5.66
1/8 MPH- 128.29
1/4 ET- 8.70
1/4 MPH- 161.82
Race weight was around 3,725lbs. Boost peaked at 26.5psi.
Now for the scary part. (Short as possible)
Our local track Kilkare has a very short shutdown. Well on this pass the chute got tangled up and didn't help to slow the car at all. I stood on the brakes and ended up melting the brake pad and backing plate on the passenger side. The piston ended up coming out and lost my front brakes. The backs then locked up. By this time I knew I was going in the sand
so I started heading to the right so I could cut left and keep the turbo from sucking in sand. I cut left at the last moment and the *** end of the car came around and slid into the sand stopping the car. Luckily we have a race/parts car in the garage with a good caliper and rotor. So we'll be good to go by the end of the weekend.
Then it will be time to see what she'll do with 100lbs out of her.

BTW, if you suck some sand in, just send the turbo our way....lol
Hope everything goes well with replacement car.I have a ? about an Ohio car I might buy you should know the car. PMing you.
Dave
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why are you putting the Th210 in the CE, whats was wrong with the 4l80e, if you dont want it you can donate it to me, or just let me borrow it.
btw what converter are you using?
glad you didnt bust this one up to, guess steve is the only one to do that
why are you putting the Th210 in the CE, whats was wrong with the 4l80e, if you dont want it you can donate it to me, or just let me borrow it.
btw what converter are you using?
glad you didnt bust this one up to, guess steve is the only one to do that

Were putting the TH210 in it to be more competitve at Milan in the Drag Radial class. It's lighter. The gearing is better and the easy stage will help me get up on boost easier. This is only temporary. Will run it this way with this motor and for a short while with the new motor. Then the 80 will go back in to get ready for Drag Week.
We run Midwest Racing Converters.
Deffinately would have sucked to have two busted cars in the garage.
Everyone was saying how they would have been scared and freakin out. But it is different when your in the situation. All I could think of was how would be the best way to get it stopped with the least damage.
Do your 150/160's make you go through plugs a lot?
You just may changed my mind about the 370 iron setup.
Plus I like to push things to the limit and make things work that shouldn't.
Who builds the motor has a lot to do with how well they take abuse. Oil pressure is still the same as the 1st pass and it has very little blowby. As soon as the new motor is done this one will be tore down and inspected. W2W or myself will post the outcome.


Glad to hear there was no major damage, I would've
my pants. 




