Cracked block and broken piston..
New forged 346ci is on the way...

Man I'm dirty...
It lasted a year though. Ever since I installed the blower, I've been gathering parts here and there when good deals came up for sale. Comming back bigger and better..Motor details
346ci, Eagle LS1 6.125" rods, Diamond -8.6 dish pistons, stock crank, new LS6 block, ARP head bolts, custom ground Comp Cam 226/232 116LSA, Texas speed CNC LS6 stage 2.5 heads 2.04intake 1.575 exhaust valves, Will put me right at 9.5:1 compression...
My "to do list"
Pull old motor.
Build and install new motor. forged 346ci.
Port match new heads to intake.
Install new aluminum flywheel and Textrillia clutch.
Install bell housing blanket...
Install DTE tranny brace and left hardened output shaft.
Install hurst shifter.
Install Wolfe 6pt cage
Install Meth inj. system.
Install smaller pulley on blower..
Install line lock..
Install new stainless brake lines..
Relocate Bosch fuel pump.
Install Bilstein sport shocks.
Just a small list. I have a week off for christmas and I plan to have it up and running by then...
Last edited by chriswtx; Nov 26, 2006 at 09:43 PM.
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All it takes is a tiny bit of detonation at those power levels to bust the piston and there is a point even with no detonation they will just fail - I'm sure you were getting close to that point.
Yeah, I was thinking the same thing. It's going to be lots of fun to put back together...

I've thought about that from day one of adding the blower. I have always been real careful not to run the car hard for more than 1/4 mile, always given it at least 30min cool down between runs, kept the mixture rich 10.7:1, timing low 14degs. On the street I never get on it more than a couple of gears for just a few seconds no more than 10sec for sure. And never back to back runs on the street. I think this was just a case of the stock cast pistons combustion chamber pressure limits...Too much power...
I think its just stress riser from the factory drilled dot to mark forward caused the failure. Its a very thin point in the piston at the ring land ...
I just finished pulling apart the motor. All the rod and main bearings still look like new..




