New Car New Build PART 2
Anyhow. I went to the track tonight. Made it a hole 30minutes befoe I decided I had to run the car. Wasnt really prepared. I just lined it up babied it out of the hole and let it eat at the top of 1rst gear.
Here is the Slips:

The night didnt really go as planned. On the second run you can see that the MPH really dropped off. Trouble stuck again. I blew the pressed in upper radiator hose out of the water pump. Never seen that one before. Anyway, the MPH shows the car has potential. I just have to get everything sorted out. Both runs were on 7lbs of boost, 11.5:1 A/F, and 17* degrees of timming.
Last edited by wickedred; May 13, 2007 at 01:15 AM.
. It felt nice to be able to run the car. I wish the second pass would have stayed together. It felt real good. I just have to get the car moving the first 60'. Been a while since I was int a turbo car. Gotta get used to it again. I topped off the tank with 110 leaded before going to the track. I still have alot of tunning to do and suspension adjustment to make. I just have to keep all the other little things in check first. Last edited by wickedred; May 13, 2007 at 01:16 AM.
For what its worth. the interstate log showed 11.5A/F, TPS 70%, MAP 180's, Timming 17*, Inj DC 89% (Motorn 60's).
.If I can get it on the dyno I will have pics and vids as well as the graphs.
Wish Me Luck.
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