LT1-LT4 Modifications 1993-97 Gen II Small Block V8

LT1 cutting out and hesitating

Thread Tools
 
Search this Thread
 
Old 09-06-2004, 09:00 AM
  #1  
On The Tree
Thread Starter
iTrader: (2)
 
Red12secZ28's Avatar
 
Join Date: Oct 2002
Location: Newport News, VA
Posts: 164
Likes: 0
Received 0 Likes on 0 Posts
Default LT1 cutting out and hesitating

I have a friend who's lt1 transam starts to hesitate and then the engine cuts off. We put a new opti spark and a new ignition module. The dam thing still wants to buck and jerk then after a few minutes the engine jsut dies. Can it be the ignition coil. We haven't replaced that yet. Its pulling a check engine light. I don't if It doesn't have any silent codes. It is a 95 where it is obd1 and the connector is obd2. I have autotap but that does me no good on his car.
Old 09-06-2004, 12:00 PM
  #2  
TECH Addict
iTrader: (2)
 
OneMeanZ's Avatar
 
Join Date: Nov 2003
Posts: 2,303
Likes: 0
Received 0 Likes on 0 Posts

Default

Could be the coil.........but I'm not sure
Old 09-06-2004, 12:33 PM
  #3  
TECH Resident
iTrader: (3)
 
Snow Dog's Avatar
 
Join Date: May 2004
Posts: 895
Likes: 0
Received 1 Like on 1 Post

Default

doubt it. go to autozone and find out what the check engine light is. does it take a few minutes for the engine to start bucking and jerking or does it do it right away? id look at the O2 sensor first, thats why you need to have the code read.
Old 09-06-2004, 07:09 PM
  #4  
TECH Fanatic
iTrader: (9)
 
Gloveperson's Avatar
 
Join Date: Feb 2004
Posts: 1,714
Likes: 0
Received 0 Likes on 0 Posts

Default

Could be a problem with fuel delivery, too.

-Todd
Old 09-07-2004, 09:28 AM
  #5  
TECH Fanatic
iTrader: (6)
 
hourang's Avatar
 
Join Date: Nov 2003
Location: Commerce Twp, MI
Posts: 1,516
Likes: 0
Received 0 Likes on 0 Posts

Default

plug wires?
Old 09-07-2004, 11:42 AM
  #6  
STF Veteran
 
TA TED's Avatar
 
Join Date: Jul 2002
Location: Beamville, VA
Posts: 784
Likes: 0
Received 0 Likes on 0 Posts
Default

After changing/checking the coil, swap MAFS with someone. I had a similar problem and the MAF was the culprit.
Old 09-07-2004, 12:36 PM
  #7  
On The Tree
Thread Starter
iTrader: (2)
 
Red12secZ28's Avatar
 
Join Date: Oct 2002
Location: Newport News, VA
Posts: 164
Likes: 0
Received 0 Likes on 0 Posts
Default

My friend said he sprayed throttle body cleaner in the throttle body and it helped clear the hesitation up. Still hick-ups though.
Old 09-07-2004, 02:19 PM
  #8  
STF Veteran
 
TA TED's Avatar
 
Join Date: Jul 2002
Location: Beamville, VA
Posts: 784
Likes: 0
Received 0 Likes on 0 Posts
Default

Throttle position sensor, Idle air control motor could be culprits if a little spray in the TB helps. That or possible dirty injectors.
Old 01-27-2005, 08:30 PM
  #9  
Cal
TECH Veteran
iTrader: (1)
 
Cal's Avatar
 
Join Date: Feb 2003
Location: Northern Utah
Posts: 4,692
Likes: 0
Received 3 Likes on 3 Posts

Default

How was this problem resloved? Mine just started doing the same damn thing tonight. Opti, ignition module, plugs & wires are relatively new. This one is a '93 though, so I don't think it has a MAS. Runs and idles fine until you try to accelerate , then it misses and cuts out. Oh, and there is no check engine light.
Old 01-27-2005, 09:53 PM
  #10  
TECH Addict
 
Poik's Avatar
 
Join Date: May 2004
Location: Bellingham/Edmonds, WA
Posts: 2,564
Likes: 0
Received 0 Likes on 0 Posts

Default

Originally Posted by Cal
How was this problem resloved? Mine just started doing the same damn thing tonight. Opti, ignition module, plugs & wires are relatively new. This one is a '93 though, so I don't think it has a MAS. Runs and idles fine until you try to accelerate , then it misses and cuts out. Oh, and there is no check engine light.
I'd say first check all the plug wires. Do you have headers?
Old 01-28-2005, 12:20 AM
  #11  
Cal
TECH Veteran
iTrader: (1)
 
Cal's Avatar
 
Join Date: Feb 2003
Location: Northern Utah
Posts: 4,692
Likes: 0
Received 3 Likes on 3 Posts

Default

Nope, no headers. It's the wife's ride and she insists we keep the car 100% stock. The plug wires have been on there a year. I'm going to get a mirror and a bright light and see if any of them are getting cooked, but they are GM wires on all the factory wire looms, so it's doubtful.
Old 01-30-2005, 11:16 PM
  #12  
Cal
TECH Veteran
iTrader: (1)
 
Cal's Avatar
 
Join Date: Feb 2003
Location: Northern Utah
Posts: 4,692
Likes: 0
Received 3 Likes on 3 Posts

Default

Well I got it fixed, so I thought I would follow up here so others may benefit. After replacing both O2 sensors then the fuel filter, the problem ended up being the fuel pump. And replacing a fuel pump in an fbody is no fun, as most of you know. It only had about 12 psi of fuel presure, not the 42 psi or so it's supposed to be. I should have checked the fuel presure before I changed that other stuff.

Last edited by Cal; 01-31-2005 at 01:21 AM.
Old 01-30-2005, 11:20 PM
  #13  
TECH Junkie
iTrader: (1)
 
FIREHAWK #07's Avatar
 
Join Date: Nov 2004
Location: TX
Posts: 3,215
Likes: 0
Received 0 Likes on 0 Posts

Default

i know you already fixed it, BUT wanted to know how many miles you had on your car..... before you changed the fuel pump. Mine is almost going to hit the 90K mark, wanted to see how many before I have to change the fuel pump
Old 01-31-2005, 01:15 AM
  #14  
Cal
TECH Veteran
iTrader: (1)
 
Cal's Avatar
 
Join Date: Feb 2003
Location: Northern Utah
Posts: 4,692
Likes: 0
Received 3 Likes on 3 Posts

Default

164,000 miles. But I'm sure it has not been operating at peak efficency for quite some time. It would cut out on occation, but we couldn't figure out what was causing it since the opti and ignition module had already been replaced. It finally got so bad the car wouldn't go over 20 mph. How humiliating for a proud Trans Am. I think if you measured the fuel presure from time to time, it would give you some advance warning of failure.

Last edited by Cal; 01-31-2005 at 01:22 AM.
Old 01-31-2005, 08:36 AM
  #15  
Teching In
 
900DollarZ's Avatar
 
Join Date: Jan 2005
Posts: 26
Likes: 0
Received 0 Likes on 0 Posts
Default

I just bought my Z28 recently and the previous owner had the fuel pump replaced after roughly 120K miles.
Old 01-31-2005, 09:10 AM
  #16  
Cal
TECH Veteran
iTrader: (1)
 
Cal's Avatar
 
Join Date: Feb 2003
Location: Northern Utah
Posts: 4,692
Likes: 0
Received 3 Likes on 3 Posts

Default

Damn you got a killer deal for $900, that's a beautiful LT1 car. That female must have thought these cars are shot after 100k miles; that couldn't be farther from the truth. I miked the cylinders for wear on my car at 145,000 miles, and they were very close to factory tolerances. Exhaust valves were a little pitted, but not that bad.
Old 01-31-2005, 01:31 PM
  #17  
TECH Fanatic
iTrader: (7)
 
67SS&99SS's Avatar
 
Join Date: Feb 2004
Location: Georgia
Posts: 1,260
Likes: 0
Received 4 Likes on 3 Posts

Default

try the coil wire. my uncle's lt1 cut out under 1/2 throttle or more, and this fixed it right up. I think it is about 20 bucks at the dealership.



Quick Reply: LT1 cutting out and hesitating



All times are GMT -5. The time now is 09:19 AM.