Fuddle 3000 Q's

). If you have time today, you can take me and the laptop for a ride and let me see/feel this issue. Never seen a small stall need the apply/release table modified but I am sure theres plenty left in the world I havent experienced. Trending Topics
Sorry about the cable issue. How was your Maui trip?
Brian
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I know if the min/max MAP boundaries are tripped it makes the trans act funky. Did you guys open the throttle blade any? If so was the TPS reset and does it fall inline with max mV? So many things to do.
Didn't mess with min/max MAP, looked a bit higher than stock but I can't remember. He's idling at 850rpm with 55-60 kPa. No DTC is set for being out of the MAP boundary.
Didn't open the tb, only adjusted RAF. RAF is a bit on the high side, but he was ok with it and it settles into idle cleanly.
The bucking is only in the 35-45 mph range or there about. I watched spark and fuel while it was bucking hoping it was just a simple fix, but they both were holding steady. It feels like the converter might be in between lock up and slip (does this sound right?). I've read threads with similar issues, and raising the lockup mph was recommended. I didn't change any of the trans settings though.
The spark dip is separate from the bucking. It only occurs while accelerating through 16-17mph and lasts for about .5 sec. Sometimes spark drops to zero, and sometimes around 5*. He has trouble repeating it, but it always occurred at slight accel through 16-17mph with tps <20%.
He had a couple of other issues that I managed to work out on Friday. His ENG SENS fuse was blown, effectively disabling the MAF and O2s. I found out the passenger side front O2 heater ground pin on the engine harness side had pulled out of its socket and wasn't making a connection anymore. Re-pinned the connector and replaced the fuse and everything seems ok. He did decide to keep his old O2s for a while longer instead of my new ones.
Car's are a whole new world......Charlie, im still with T-mobile. I sent the other phone back cause I was having way too many issues with it.
Let me know once Brian loads the new TCC table in if there is anymore problem. Since I didnt log it we may have to adjust a hair here or there. Omar was able to reproduce the drop in timing/hesitation, which Andrew used to have the same issues long long ago. I will fix it and send it back to you, with a list, or you simply look at the log history to see where I went and changed




