Many 4l60e problems
Put aftermarket 3500 converter in, ran good, had it tuned. Had about 20 track passes and 500 or so miles on it. Felt a vibration so had it replaced to possibly cure vibration issues. While it was out had transmission rebuilt, was working properly before, with about $1300 in parts from transmissioncenter(all the good stuff).
So anyways got a new aftermarket converter, put it in, now after rebuild the new converter felt extremely loose and car would not shift at WOT into 3rd gear or 4th. 1-2 shift was fine.
So pulled it back out and had it gone through again, couldn't find anything wrong. Replaced overrun and 3-4 clutches. Same thing happened again. So after only 1 mile of driving hoping there was not too much harm put the stock converter in and it ran fine. (thinking this whole time it's a converter issue) Shifted fine/drove fine/no problems. Except about 1000 miles later it started bearly slipping into OD on easy driving. So pulled it back out and had it gone through again. The hardened input shaft was replaced with the stock one maybe thinking it was the problem, and 3-4clutches again.
So I now drove it for about a year, about 3-4000 miles with no issues. Shifts perfect, tons of WOT passes.
Took the car out tonight and immediatedly lost 3rd and 4th gear again. 1st and 2nd are still fine. 3-4 are totally gone.
So now obviously I know it's not a converter issue. The fluid kept smelling burnt, but I didn't know if it was just from the maybe 1 qt that I couldn't get out of the stock converter. Anyone have suggestions to as what could be slowly causing my 3-4 clutches to burn up or as to why only with the larger converter it burns them up immediately.
I can't name all the parts put in the tranny at the rebuild but obviously something is not right.
Is this a common used part?
https://transmichigan.com/catalog/pr...products_id=50
I had one person question it.
Thanks for any help
As for the check valve by sonnax I havent used it so I do not know about its effect on long term durabilty, I do know its very important to get the 2-4 band off quickly to avoid overlap or the 3-4 clutch will die quickly , Each builder has a different way of working to assure that But I think all will agree its very important and overlap does seem likley the cause in your case.
They were upgraded clutches, red alto the first time, but the 2nd and 3rd they were just stock ones I beleive, bc that would've been 80 bucks each time, and I was hesistant.
They said the leaking pressure on the 3-4 clutches was probably the issue too.
The car was in there air, and checked the pressure before it got taken out.
park 75psi at idle
120-160 reving around 2k
nuetral was the same
reverse 220 at idle
manual first it had 65 just idling
then 160psi around 2000rpms
manual 2nd had 160psi around 2000rpms
It did grab 3rd gear in the air with no load on it and around 2000rpms is was only 70psi.
Didn't go fast enough to hit OD in the air.
I don't know what is normal for each gear, I know reverse is supposed to be high. The lower psi in 3rd seemed odd. But I was getting the results for the tranny shop, they wanted to know.
brake torquing in the air to about 1200 rpms in manual first was around 150-155psi.
The transmission is out, so I can't test anymore. I'm probably going to have my hardened input shaft put back in bc now its just a $295 paperweight til it goes back in. It was removed thinking it could've been the problem on the last rebuild. But I'm sure this shop will check it. The fluid is obvisously smoked.
I'll get some results up when its apart. If they can't find anything wrong either I guess my option is to just have the input drum put back to stock parts? unless it's in the valve body.
Now my hardened one is going back in knowing it was never the problem.
hopefully I have some luck, I'll update when it's in the car with the new yank 3600
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The reason I ask is there may be a fix for it. We, and several other builders utilize a sleeved input drum. Whereby a steel sleeve is placed around the hub that keeps it from expanding, which could cause a pressure leak at best and a frcture at worst.
It could have been cracked during the removal and installation of the input shaft previously as well.
Good Luck.
g
The hardened one has that sleeve in the middle of it already. Thanks
Right.... that's what I was trying to get at. If the drum broke at the snap ring landing that could easily be related to the original issues.
Have your builder take a look at the feed holes in the valve body plate. I will bet the 3rd feed hole is too large... just an observation based on info presented though. Those snap rings do not ordinarilly blow out.
Good info. thanks for getting back to us.
g
was drilled out to match it like the instructions said. I thought one more was, but I just watched/helped the builder at the time, so I could be wrong, I'll ask the shop about it when I take the overrun piston and spring that I needed for that hardend input drum(With the sleeve), the ones I had I guess got misplaced so I have to wait on them to come.
I still can't figure out the vibration. It really almost seems to be gone now with the transmission out. I have the prothane motor mounts here now..but don't see why that would do anything really.
It was a stock flexplate and converter. And obviously the flexplate is still attached in order to start the car.
Has anyone ever seen something inside a transmission cause a vibration. Who knows, if I had a spare tranny i'd stick it on just to eliminate the transmission.
I'll get updates after it's running in a few days.
If you're cruising around 60 or so you can feel it slightly, it's always there. Then I can throw it in nuetral and it goes away.
The reason I asked this was to determine whether we should concern ourselves with the pinion angle or not. I believe we should based on your last answer.
Check and verify that the pinion angle is correct. Also, check the torque arm to ensure that it is attached properly.
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