Mis-Fire...
It started up ok, warmed up ok.. then drove some and then it started to happened. A mis-fire, like once in a while, Not constant but every once in a while or one or two.. then nothing for a bit. Seems to only happen when at running temp.
I swapped out the Cam sender.. no change, still there. Changed out the coil pack, no change again. Thinking it might be the Crank sender as it might have gotten wet while I was cleaning the engine up before it reinstalled everything.
check all of the grounds and they were connected and tight to the block, frame and body. Checked all of the connectors (injector, coil, TPS, ECT, etc...) Couldn't find anything.
No DTC codes being stored !
I connected my monitor and watch the O2 info and fuel trims. A bit funny reading. But then might have always been a bit off balanced between sides.
Anyway..
Voltage is constant on bank 2 at 0.4 at idle and high idle. Bank 1 varies between 0.1 and 0.8
Short Term fuel trim and Fuel trim on bank 2 stand fairly constant 0.0 - 0.8 with Bank 1 jumping up and down at the O2 voltage changes up to 2 or 3 percentage.
Long Term Fuel trim is around 0.8 on Bank 2 with Bank 1 at 12.5 to 14.8. Large difference.
I am looking for input on possible direction to keep looking. Also hear something funny when listening to the exhaust on the Left side (bank 1).. some slight pinging !? but not on the Right Side (bank 2). I also suspect that the problem is on the left side/bank1 as when I am listening to the engine (inside the engine bay). I hear the pop of the mis-fire and think I hear it from the rear of bank 1 (#7 and #5 ?), But that could just be the sound traveling out and down the headers.
Change Bank 2 O2 ?
Change Crank position Sender ?
Any suggestion on other things to try and isolate ?
thanks
BC
I had an odd misfire in my WS6 that ended up being a bad PCM. Mine would give me a code that said "Cylinder 5 Misfire," but only intermittently.
Essentially there was no spark on cylinder 5 most of the time. I flashed my current tune on a spare PCM and installed it in the car - problem sorted. I moved the PCM to another car and the intermittent misfire followed. Ironically the WS6 was completely stock at the time. I have HP Tuners which includes an awesome scan / logging utility that helped me find the problem and flash the spare PCM. I think I would have spent a lot of time if I didn't have the real time scan feature.
Just ideas for you. Good luck.
So don't forget the basics, like a loose hose or connector, vac leak, stuck or dirty injector-throttle body-IAC valve, low fuel pressure, dirty fuel filter. Couldn't hurt to pull your plugs and clean them if needed.
As for the cam sensor, if the stock computer is anything like the ignition controller for carbd vehicles than the cam position sensor isn't needed once the car is running. It merely sets the phase at start up. You can usually unplug them once running.
Good luck on this one, I hate electrical gremlins. Let us know what you ultimately find out.
- Fuel pressure is good at both idle and high idle, throttle being varied to high and low throttle quickly. Can do a WOT during the drive test (as long as it doesn't mis-fire).
New plugs
- Connector was crimped with new terminal, no extra wire was needed so no soldering involved. Checked with a DVM from connector to PCM Connector.
- Coil pack was swapped with plug wires
- Checked for vacuum leaks
- Intake gaskets and Injector O-Rings (injectors were not removed from the intake/rail) are good, was replaced a little over a year ago the last time I changed the oil pan out.
- checked under the valve cover for any broke spring or loose rockers.
Like you all said and suggested. I have done the basic a few times.. but without a good high end scanner, I will not be able to get a good deep scan. I do know I am not getting any codes.
Looking for more suggestion.. I might have to take it to a shop ??
thanks guys..
BC
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Using MAF, will check it again and spay clean with MAF Cleaner. Might also try disconnecting it once it warms up to see what happens.
O2, I'll try swapping them over or with some spares. As I originally posted, the reading between Bank 1 and 2 were way different.
Thanks guys
BC
Before you do all that, did you a crank relearn after you put the new camshaft sensor in?
http://www.hptuners.com/forum/showth...=crank+relearn
thanks for the info and suggestions.
BC
One think I was a little alarmed about was the Bank 2 voltage.. it was at 0.4 steady.. found I had used the PID for the Display. After correcting it. Found that the Voltage was moving as it should like Bank 1 now.
What is still alarming.. is the higher LTFT on Bank 1.. it at times is still 14.8 %.. as compared to Bank 2 which at a much lower percentage.
I have been listening to the popping sound from the tail pipe. The popping is coming from the Bank 1 side..I am wondering if I have a valve problem ? I don't hear any ticking at the engine so maybe it is a burn valve ? Well take the valve cover off again Friday if I have time. Also might try a leak down test to see what the seal is on the valve and rings.
Will keep trying to isolate the problem. But any input on anything would be helpful from you guys.. thanks..
BC
just ging to keep gacking away. It is just time comsuming with no results.
Thanks
BC
Last edited by bczee; May 30, 2014 at 10:51 AM.
Oh well, upgrading to Aeromotive pump and a brand new sender assembly.
Nice to finally see results on this issue since I have been trying to track down the problem for 3 years.
Oh well, upgrading to Aeromotive pump and a brand new sender assembly.
Nice to finally see results on this issue since I have been trying to track down the problem for 3 years.
Lucky I had the Trunk Access panel, was able to open it up without dropping the tank, remove the sending unit and found the blacken connector. I cleaned it up. replaced what was needed and secured the terminal and connector and back on the road in no time thanks to the access panel. I know I had posted or informed other on some thread for this before.. to bad you didn't pick up the issue that I had.. would have saved you a few years of your life ! LOL..
BC






