LQ4 into a 3rd Gen/1972 Nova
The Best V8 Stories One Small Block at Time
I had to resort back to the previous thinner rad and run dual 1750cfm fans.. which seems to keep the engine running consistently cool at ~185-190*F after boosty pulls to quick stops on the street. Idling it was holding about 175*F.
To get maximum clearance of passenger side fan to the hotside pipe, I reverse mounted the fan from the inside of the shroud, and clearance cut out the plastic ring between the mounting tabs, to allow airflow between the mounting tabs. The pictures will make it make more sense..
Also picked up my new turbo on Dec 24.. merry xmas to me!! I also got a 800hp Mcleod twin plate RST clutch, a bigger 46mm Precision wastegate, and a turbo blanket. The turbo magically dropped right into the piping I had fabricated around the TC76, so no T4 flange or downpipe vband flange mods were needed. Since the outer diameter of the turbine housing is bigger and closer to the hood, I got the turbo blanket. Finally, the all-important turbo stats are: PTE 7675 CAE CHRA 0.96 A/R.. oi what a mouthful. Translation: billed compressor wheel, ceramic bb center section, and a ceramic coated turbine housing. This thing is gonna be silly.
Last edited by frojoe; Dec 28, 2014 at 07:20 PM.
Started it up and with the BB turbo (with factory Precision oil restricor) the engine was giving 55psi cold oil pressure, 45psi warm, and almost 90psi when revving the engine.. hooray!
But realistically.. when am I ever going to be in said "high rpm low boost" scenario?!? That would just be silly.

It passed all the required tests:
- drivethru test
- grocery-getting test
- "four spare tires in the trunk" test
- idling and other car guys think "just got a tree-fitty in it" test
- 3rd and 4th gear "highway passing power" test
- "cops drive by it without a second glance or suspicion" test
But then.. the Aeromotive 340 fuel pump fails and leaves me stranded. Need to pull the tank and see if it's the in-tank pump ground or power wiring that's failed, or the pump itself that failed. Either way I have two Walbro 255's on the way so this doesn't happen again. At least the tow truck driver was a cool old timer with a ton of musclecar stories, and was respectful/careful with the car and good with the truck boom..



Good luck getting everything fixed and back on the road soon!
I haven't put the Mcleod yet, waiting on Tremec F-body Magnum to be released then I'm going to pull the whole engine/trans install clutch at that time, as well as fix the porous old weld on the front of the oil pan that is slowly wicking oil and driving me nuts.





