Projekt Lazarus - Numbers Posted!!
Originally Posted by Launch
I agree. Once properly sorted (the fouled spark plug issue) this will be a wicked n/a street car. I'm thinking of traction difficulties though.. same as with your 434ci and your car. I think if we ever get out of this covid lockdown, a chassis shop and tubs are in order. I was thinking of doing it to mine before the covid bs began. Darth could probably do a whole custom 1/2 chassis rear clip on his car with some 31"x18.50" hoosier QTP tires under there and not get hassled by police over legality like we do over in australia? Imagine all that traction on the street from the hit....
I'd never do that to my Miata. It's intended to turn corners, and it wouldn't turn corners on giant drag slicks. I know I give up straight line capability (I'm on 225 street radials, LOL), but I don't care.
Thread Starter
Joined: Jul 2014
Posts: 10,451
Likes: 1,872
From: My own internal universe
Guys thank you for all the kind words. Both very humbling and very much appreciated. There is so much to reply to and yest, to try would just be a multiquote from hell. I had to catch up on stuff around the house, so I have pretty much parked it since Friday evening. Got family coming over today. Life steps in, etc.
To answer the big question, next steps -- I really need to get the intake off and see what's going on in port 3. Tony's choo-choo-train comment is not far off actually. I put a vid on here from day 1 when we were trying to handle some weird breaking up at 2800 it wants to do. I stepped out of the car and the guy held it at that spot. My hope is it is nothing but an epoxy failure and I can re-epoxy it and it holds better. We will see, anyway. But it sucks to drive and then your clothes smell like burnt oil the rest of the day, so I gotta fix that before I do much else. It's also impossible to tell what is ring seal and what is leaking in.
I also put a vid in that everyone wants to se. Pull #6 from day 1. You can tell at the end of the pull, it was still pulling hard. I drove all the dynos day 2, and I was preoccupied with trying to make equipment changes quickly since I was paying by the hour. But anyway, enjoy!
To answer the big question, next steps -- I really need to get the intake off and see what's going on in port 3. Tony's choo-choo-train comment is not far off actually. I put a vid on here from day 1 when we were trying to handle some weird breaking up at 2800 it wants to do. I stepped out of the car and the guy held it at that spot. My hope is it is nothing but an epoxy failure and I can re-epoxy it and it holds better. We will see, anyway. But it sucks to drive and then your clothes smell like burnt oil the rest of the day, so I gotta fix that before I do much else. It's also impossible to tell what is ring seal and what is leaking in.
I also put a vid in that everyone wants to se. Pull #6 from day 1. You can tell at the end of the pull, it was still pulling hard. I drove all the dynos day 2, and I was preoccupied with trying to make equipment changes quickly since I was paying by the hour. But anyway, enjoy!
My car did the exact same thing on the first 2 pulls. On the third pull it was just like someone hit a switch and the smoke just quit instantly and never returned. I was a little worried at first though for sure.
Thread Starter
Joined: Jul 2014
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From: My own internal universe
Originally Posted by 01CamaroSSTx
Yup she's burning oil alright...

Originally Posted by Bspeck82
Maybe just missed/forgot to silicone the rocker bolt for that port?
Originally Posted by Double06
Do these heads have a through bolt into intake port from rocker arms?
Originally Posted by ramairws6
My car did the exact same thing on the first 2 pulls. On the third pull it was just like someone hit a switch and the smoke just quit instantly and never returned. I was a little worried at first though for sure.
If everyone remembers I missed the lifter cut with the pushrod, bent the rod, bound up and broke the link bar, spun the lifter, and the busted link bar punched a hole in the intake runner from underneath. All that happened on number 6.
We epoxied it, and my fear is the early overheat issue I was having after THIS first start caused the epoxy patch to fail. I moved the head to driver side because on a F car that is the easier side. Which means the epoxy patch would be on 3, which is the one that is oil fouling in a single pull.
I was going to wait until I got the intake off to confirm it and post knowledge vs speculation but thought I would at least remind everyone what happened before.
Here's how #3 looked every pull even after putting a brand new plug in.
Thats the problem with repairs like that. Always seems 50/50 and will be in the back of your mind forever. I for sure would have bought a new head knowing I just dont get lucky like that. But hey, he took a shot. At least Jake is transparent and we ll 100% know for sure soon.
Good luck with your investigation next week here. BTW your 7,000 rpm torque is 90% of your 5,000 rpm tq which is outstanding (480/530 - I am going off your 650 hp run), the later ones were even better.
Thread Starter
Joined: Jul 2014
Posts: 10,451
Likes: 1,872
From: My own internal universe
Thats the problem with repairs like that. Always seems 50/50 and will be in the back of your mind forever. I for sure would have bought a new head knowing I just dont get lucky like that. But hey, he took a shot. At least Jake is transparent and we ll 100% know for sure soon.












